A failed main rotor blade fork (big) of a helicopter was forwarded to this laboratory for analyzing the cause of failure. Examination revealed that the bolt has failed by fatigue. There was multiple fatigue crack initiation on the threads of the bolt. After initiation, a few of the cracks joined together to form major fatigue crack fronts which then propagated progressively over about 95% of the cross section before culminating in static overload failure. Evidences suggest that there was relative movement (slip) between the nut and the bolt which resulted in thinning of the threads on the bolt by wear process. Because of reduction in cross section, the load carrying capacity of the threads reduced drastically leading to initiation of a numb...
Two fractured main landing attachment bolts from an aircraft were sent to the laboratory for analysi...
Two fractured main landing attachment bolts from an aircraft were sent to the laboratory for analysi...
Support assembly of a fractured tail under carriage a helicopter was sent to the laboratory for anal...
A failed main rotor blade fork (big) of a helicopter was forwarded to this laboratory for analyzing ...
A cracked titanium alloy ‘bolt-blade fork’ of main rotor assembly of a helicopter was analyzed. Anal...
A cracked titanium alloy ‘bolt-blade fork’ of main rotor assembly of a helicopter was analyzed. Anal...
A failed bolt of horizontal stabilizer support (RH) of a helicopter was analyzed. Analysis showed th...
A failed bolt of horizontal stabilizer support (RH) of a helicopter was analyzed. Analysis showed th...
A failed main gear leg of a helicopter was analyzed. Fractographic study confirmed that the failure ...
The lugs of the main rotor blade fork assembly have failed by wear followed by fatigue. The to and f...
The lugs of the main rotor blade fork assembly have failed by wear followed by fatigue. The to and f...
A prematurely failed hub plate lower made of titanium alloy belonging to the tail rotor assembly of ...
A prematurely failed hub plate lower made of titanium alloy belonging to the tail rotor assembly of ...
A damaged input pinion, part No. 201P 636H 1302 201 bearing Sl. No. HDSN 527, belonging to Advanced ...
AbstractA military helicopter crash was investigated. The aircraft was flying at cruise speed in cle...
Two fractured main landing attachment bolts from an aircraft were sent to the laboratory for analysi...
Two fractured main landing attachment bolts from an aircraft were sent to the laboratory for analysi...
Support assembly of a fractured tail under carriage a helicopter was sent to the laboratory for anal...
A failed main rotor blade fork (big) of a helicopter was forwarded to this laboratory for analyzing ...
A cracked titanium alloy ‘bolt-blade fork’ of main rotor assembly of a helicopter was analyzed. Anal...
A cracked titanium alloy ‘bolt-blade fork’ of main rotor assembly of a helicopter was analyzed. Anal...
A failed bolt of horizontal stabilizer support (RH) of a helicopter was analyzed. Analysis showed th...
A failed bolt of horizontal stabilizer support (RH) of a helicopter was analyzed. Analysis showed th...
A failed main gear leg of a helicopter was analyzed. Fractographic study confirmed that the failure ...
The lugs of the main rotor blade fork assembly have failed by wear followed by fatigue. The to and f...
The lugs of the main rotor blade fork assembly have failed by wear followed by fatigue. The to and f...
A prematurely failed hub plate lower made of titanium alloy belonging to the tail rotor assembly of ...
A prematurely failed hub plate lower made of titanium alloy belonging to the tail rotor assembly of ...
A damaged input pinion, part No. 201P 636H 1302 201 bearing Sl. No. HDSN 527, belonging to Advanced ...
AbstractA military helicopter crash was investigated. The aircraft was flying at cruise speed in cle...
Two fractured main landing attachment bolts from an aircraft were sent to the laboratory for analysi...
Two fractured main landing attachment bolts from an aircraft were sent to the laboratory for analysi...
Support assembly of a fractured tail under carriage a helicopter was sent to the laboratory for anal...