A prematurely failed hub plate lower made of titanium alloy belonging to the tail rotor assembly of a helicopter was sent to the laboratory for analysis. Examination revealed that a fatigue crack initiated at the web radius region and propagated progressively through thickness. Non-uniform loading was observed on the blade-side surface of the hub plate around the bolt hole corresponding to blade-G. Damages in the form of rubbing were also observed on the inner surface of the hub plate indicating misalignment of this component with the tail rotor shaft. It appears most probable that this misalignment has resulted in assembly stresses leading to fatigue crack initiation. There were no evidences of metallurgical or mechanical abnormalities at ...
The control tube has failed by rotating bending fatigue. Fretting was observed on the contacting sur...
Evidences suggest that the mechanical damage that got created on the bore inner surface during fatig...
The control tube has failed by rotating bending fatigue. Fretting was observed on the contacting sur...
A prematurely failed hub plate lower made of titanium alloy belonging to the tail rotor assembly of ...
A failed main gear leg of a helicopter was analyzed. Fractographic study confirmed that the failure ...
Support assembly of a fractured tail under carriage a helicopter was sent to the laboratory for anal...
A failed main rotor blade fork (big) of a helicopter was forwarded to this laboratory for analyzing ...
A failed main rotor blade fork (big) of a helicopter was forwarded to this laboratory for analyzing ...
A cracked titanium alloy ‘bolt-blade fork’ of main rotor assembly of a helicopter was analyzed. Anal...
A cracked titanium alloy ‘bolt-blade fork’ of main rotor assembly of a helicopter was analyzed. Anal...
Support assembly of a fractured tail under carriage a helicopter was sent to the laboratory for anal...
A cracked ARIS casing ring belonging to a helicopter was forwarded to this laboratory for analysis. ...
A cracked ARIS casing ring belonging to a helicopter was forwarded to this laboratory for analysis. ...
A failed bolt of horizontal stabilizer support (RH) of a helicopter was analyzed. Analysis showed th...
A failed bolt of horizontal stabilizer support (RH) of a helicopter was analyzed. Analysis showed th...
The control tube has failed by rotating bending fatigue. Fretting was observed on the contacting sur...
Evidences suggest that the mechanical damage that got created on the bore inner surface during fatig...
The control tube has failed by rotating bending fatigue. Fretting was observed on the contacting sur...
A prematurely failed hub plate lower made of titanium alloy belonging to the tail rotor assembly of ...
A failed main gear leg of a helicopter was analyzed. Fractographic study confirmed that the failure ...
Support assembly of a fractured tail under carriage a helicopter was sent to the laboratory for anal...
A failed main rotor blade fork (big) of a helicopter was forwarded to this laboratory for analyzing ...
A failed main rotor blade fork (big) of a helicopter was forwarded to this laboratory for analyzing ...
A cracked titanium alloy ‘bolt-blade fork’ of main rotor assembly of a helicopter was analyzed. Anal...
A cracked titanium alloy ‘bolt-blade fork’ of main rotor assembly of a helicopter was analyzed. Anal...
Support assembly of a fractured tail under carriage a helicopter was sent to the laboratory for anal...
A cracked ARIS casing ring belonging to a helicopter was forwarded to this laboratory for analysis. ...
A cracked ARIS casing ring belonging to a helicopter was forwarded to this laboratory for analysis. ...
A failed bolt of horizontal stabilizer support (RH) of a helicopter was analyzed. Analysis showed th...
A failed bolt of horizontal stabilizer support (RH) of a helicopter was analyzed. Analysis showed th...
The control tube has failed by rotating bending fatigue. Fretting was observed on the contacting sur...
Evidences suggest that the mechanical damage that got created on the bore inner surface during fatig...
The control tube has failed by rotating bending fatigue. Fretting was observed on the contacting sur...