AbstractA military helicopter crash was investigated. The aircraft was flying at cruise speed in clear sky at 1000 feet over a flat area. The crew suddenly lost the control of the helicopter that crashed in the immediately causing fatal injuries to the whole crew. Four main rotor blades were found close to the impact point, while the fifth blade was found about 900 m before the wreck. Therefore efforts were directed to the failure of this blade that had apparently separated in the air. The rotor blade comprised a long hollow 6061-T6 aluminum alloy extrusion and 25 thin metallic pockets that provided the trailing edge airfoil shape. Visual examination of the fracture surface of the aluminum extrusion indicated fatigue crack growth followed b...
A few components retrieved from the wreckage of a helicopter were sent to the laboratory for investi...
Three failed compressor rotor blades, one from first stage and the other two from second stage, bel...
The aircraft met with an incident on March 23, 2006. On strip examination of the engine, one of the ...
AbstractA military helicopter crash was investigated. The aircraft was flying at cruise speed in cle...
During a sortie in a Chetak helicopter, severe vibrations were experienced. On landing, it was . no...
The fractured HPTR disc belonging to an aeroengine retrieved from the wreckage of an aircraft was in...
The main rotor blade of an helicopter which had developed cracks on the aluminium alloy skin was sen...
During a sortie in a Chetak helicopter, severe vibrations\ud were experienced. On landing, it was . ...
The fractured HPTR disc belonging to an aeroengine retrieved from the wreckage of an aircraft was in...
A Light Utility Helicopter (LUH), in the course of a training flight, leaving the ground during the ...
This paper presents the failure analysis results of the helicopter skid landing gear. The helicopter...
This paper presents the failure analysis results of the helicopter skid landing gear. The helicopter...
There was an accident to a helicopter during ground run on July 28, 2008 wherein one upper and lower...
There was an accident to a helicopter during ground run on July 28, 2008 wherein one upper and lower...
Three failed compressor rotor blades, one from first stage and the other two from second stage, bel...
A few components retrieved from the wreckage of a helicopter were sent to the laboratory for investi...
Three failed compressor rotor blades, one from first stage and the other two from second stage, bel...
The aircraft met with an incident on March 23, 2006. On strip examination of the engine, one of the ...
AbstractA military helicopter crash was investigated. The aircraft was flying at cruise speed in cle...
During a sortie in a Chetak helicopter, severe vibrations were experienced. On landing, it was . no...
The fractured HPTR disc belonging to an aeroengine retrieved from the wreckage of an aircraft was in...
The main rotor blade of an helicopter which had developed cracks on the aluminium alloy skin was sen...
During a sortie in a Chetak helicopter, severe vibrations\ud were experienced. On landing, it was . ...
The fractured HPTR disc belonging to an aeroengine retrieved from the wreckage of an aircraft was in...
A Light Utility Helicopter (LUH), in the course of a training flight, leaving the ground during the ...
This paper presents the failure analysis results of the helicopter skid landing gear. The helicopter...
This paper presents the failure analysis results of the helicopter skid landing gear. The helicopter...
There was an accident to a helicopter during ground run on July 28, 2008 wherein one upper and lower...
There was an accident to a helicopter during ground run on July 28, 2008 wherein one upper and lower...
Three failed compressor rotor blades, one from first stage and the other two from second stage, bel...
A few components retrieved from the wreckage of a helicopter were sent to the laboratory for investi...
Three failed compressor rotor blades, one from first stage and the other two from second stage, bel...
The aircraft met with an incident on March 23, 2006. On strip examination of the engine, one of the ...