A failed main gear leg of a helicopter was analyzed. Fractographic study confirmed that the failure of the leg was by fatigue. Multiple fatigue cracks were found to have initiated at the toe of the weld and propagated progressively along the thickness as well as along the circumference of the tubular construction. A general check on the material and the weld did not reveal any obvious abnormalities which could give rise to the fatigue crack initiation. However, this needs to be confirmed by comparing the material, hardness and the microstructure with those of the specification. It is stated that due to lack of information, no analysis could be attempted towards identification of the cause of failure
The IGB failure was due to fatigue fracture of the driving gear. There were three major fatigue crac...
Two cracked Main Gear-Box (MGB) housings of a particular type of helicopter were referred to the lab...
A broken tail gearbox (TGB) housing and failed pitch link assemblies of a helicopter were sent to th...
Support assembly of a fractured tail under carriage a helicopter was sent to the laboratory for anal...
Support assembly of a fractured tail under carriage a helicopter was sent to the laboratory for anal...
This paper presents the failure analysis results of the helicopter skid landing gear. The helicopter...
This paper presents the failure analysis results of the helicopter skid landing gear. The helicopter...
A cracked slithering handle was sent to the laboratory for investigation. Examination revealed that ...
A failed main rotor blade fork (big) of a helicopter was forwarded to this laboratory for analyzing ...
A cracked slithering handle was sent to the laboratory for investigation. Examination revealed that ...
A failed main rotor blade fork (big) of a helicopter was forwarded to this laboratory for analyzing ...
Out of the five control tubes referred to NAL, four were found to have cracks/indication of cracks. ...
Out of the five control tubes referred to NAL, four were found to have cracks/indication of cracks. ...
Out of the five control tubes referred to NAL, four were found to have cracks/indication of cracks. ...
The IGB failure was due to fatigue fracture of the driving gear. There were three major fatigue crac...
The IGB failure was due to fatigue fracture of the driving gear. There were three major fatigue crac...
Two cracked Main Gear-Box (MGB) housings of a particular type of helicopter were referred to the lab...
A broken tail gearbox (TGB) housing and failed pitch link assemblies of a helicopter were sent to th...
Support assembly of a fractured tail under carriage a helicopter was sent to the laboratory for anal...
Support assembly of a fractured tail under carriage a helicopter was sent to the laboratory for anal...
This paper presents the failure analysis results of the helicopter skid landing gear. The helicopter...
This paper presents the failure analysis results of the helicopter skid landing gear. The helicopter...
A cracked slithering handle was sent to the laboratory for investigation. Examination revealed that ...
A failed main rotor blade fork (big) of a helicopter was forwarded to this laboratory for analyzing ...
A cracked slithering handle was sent to the laboratory for investigation. Examination revealed that ...
A failed main rotor blade fork (big) of a helicopter was forwarded to this laboratory for analyzing ...
Out of the five control tubes referred to NAL, four were found to have cracks/indication of cracks. ...
Out of the five control tubes referred to NAL, four were found to have cracks/indication of cracks. ...
Out of the five control tubes referred to NAL, four were found to have cracks/indication of cracks. ...
The IGB failure was due to fatigue fracture of the driving gear. There were three major fatigue crac...
The IGB failure was due to fatigue fracture of the driving gear. There were three major fatigue crac...
Two cracked Main Gear-Box (MGB) housings of a particular type of helicopter were referred to the lab...
A broken tail gearbox (TGB) housing and failed pitch link assemblies of a helicopter were sent to th...