In this paper, we present the results of an extensive measurement campaign to investigate the effects of external and internal sidewall compression and variation of internal contraction on the performance and flowfield of a SCRamjet-inlet. Experiments were conducted in the H2K windtunnel of DLR Cologne at Mach 7. The performance was evaluated by static and total pressure ratios, kinetic energy efficiency and mass capture ratios. The flowfield was analysed using wall pressure distributions, Pitot pressure and Mach number profiles at the isolator interface to the combustion chamber and infrared thermography on the external ramps. The results show that the combination of a two-ramp inlet with external sidewall compression is not suitable for i...
A measurement campaign has been carried out to investigate the viscous flow effects in a fixed geome...
A computational parametric study of three-dimensional, sidewallcompression scramjet inlets was perfo...
Reynolds number and cowl position effects on the internal shock structure and the resulting performa...
In this paper, we present the results of an extensive measurement campaign to investigate the effect...
We conducted an extensive experimental examination of the operational behavior of a three-dimensiona...
We conducted an extensive experimental examination of the operational behavior of a three-dimensiona...
The current experimental study at Mach 7 was carried out to investigate the viscous flow effects in ...
We conducted an extensive experimental examination of the operational behavior of a three-dimensiona...
A compact three-dimensional scramjet intake with a high compression ratio and a movable cowl as a st...
A combination of CFD simulation and experimental comparison has been conducted for a generic three-d...
The advantages and design requirements of propulsion/airframe integration for high Mach number fligh...
The Scramjet Inlet Performance Experiment (SIPE) investigated the performance of a fully-rotated Bus...
The inlet of a Mach 8 cruise vehicle has been experimentally investigated in a hypersonic blow down ...
The inlet of a Mach 8 cruise vehicle has been experimentally investigated in a hypersonic blow down ...
The inlet of a Mach 8 cruise vehicle has been experimentally investigated in a hypersonic blow down ...
A measurement campaign has been carried out to investigate the viscous flow effects in a fixed geome...
A computational parametric study of three-dimensional, sidewallcompression scramjet inlets was perfo...
Reynolds number and cowl position effects on the internal shock structure and the resulting performa...
In this paper, we present the results of an extensive measurement campaign to investigate the effect...
We conducted an extensive experimental examination of the operational behavior of a three-dimensiona...
We conducted an extensive experimental examination of the operational behavior of a three-dimensiona...
The current experimental study at Mach 7 was carried out to investigate the viscous flow effects in ...
We conducted an extensive experimental examination of the operational behavior of a three-dimensiona...
A compact three-dimensional scramjet intake with a high compression ratio and a movable cowl as a st...
A combination of CFD simulation and experimental comparison has been conducted for a generic three-d...
The advantages and design requirements of propulsion/airframe integration for high Mach number fligh...
The Scramjet Inlet Performance Experiment (SIPE) investigated the performance of a fully-rotated Bus...
The inlet of a Mach 8 cruise vehicle has been experimentally investigated in a hypersonic blow down ...
The inlet of a Mach 8 cruise vehicle has been experimentally investigated in a hypersonic blow down ...
The inlet of a Mach 8 cruise vehicle has been experimentally investigated in a hypersonic blow down ...
A measurement campaign has been carried out to investigate the viscous flow effects in a fixed geome...
A computational parametric study of three-dimensional, sidewallcompression scramjet inlets was perfo...
Reynolds number and cowl position effects on the internal shock structure and the resulting performa...