An altitude-test-chamber investigation of a 28-inch-diameter ram-jet engine at a simulated flight Mach number of approximately 2.0 for altitudes of 40,000 to 50,000 feet was conducted at the NACA Lewis laboratory. Three different flame holders, varying in the number and size of the annular gutters, in conjunction with several fuel-injection systems were investigated. The combustion efficiency for the flame-holder fuel-injection system that provided the best over-all operational fuel-air-ratio range (0.03 to 0.075) was over 0.9 at a fuel-air ratio of about 0.065 for the altitude range investigated
Experimental investigation of engine dynamics and controls for 48-inch ramjet engine in free jet fac...
An investigation of turbojet-engine thrust augmentation by means of tail-pipe burning has been condu...
A preliminary evaluation was made of three types of combustor configurations in a 48-inch-diameter r...
The results of an altitude test-chamber investigation of the effects of a number of design changes a...
Altitude-test-chamber investigation of effects of flame-holder blocked area and gutter width on perf...
A ram-jet engine with an experimental 48-inch-diameter combustor was investigated in a free-jet faci...
An analytical investigation was made of the performance of isolated ram-jet engines in the flight Ma...
An investigation of the altitude performance of a 20-inch-diameter high-temperature-ratio ram-jet co...
An investigation was conducted with a single combustor from a J47 turbojet engine using weathered av...
As part of an investigation of the performance of AN-F-58 fuel in various types of turbojet engine, ...
A Westinghouse 24C-2 combustor was investigated at conditions simulating operation of the 24C Jet en...
An investigation was conducted in an altitude test chamber at the NACA Lewis laboratory to determine...
An altitude-test-chamber investigation was conducted to determine the operational and performance ch...
A brief investigation has been made of the performance of a single combustor of the TG-180 turboJet ...
An investigation was conducted in the Cleveland altitude wind tunnel to determine the operational ch...
Experimental investigation of engine dynamics and controls for 48-inch ramjet engine in free jet fac...
An investigation of turbojet-engine thrust augmentation by means of tail-pipe burning has been condu...
A preliminary evaluation was made of three types of combustor configurations in a 48-inch-diameter r...
The results of an altitude test-chamber investigation of the effects of a number of design changes a...
Altitude-test-chamber investigation of effects of flame-holder blocked area and gutter width on perf...
A ram-jet engine with an experimental 48-inch-diameter combustor was investigated in a free-jet faci...
An analytical investigation was made of the performance of isolated ram-jet engines in the flight Ma...
An investigation of the altitude performance of a 20-inch-diameter high-temperature-ratio ram-jet co...
An investigation was conducted with a single combustor from a J47 turbojet engine using weathered av...
As part of an investigation of the performance of AN-F-58 fuel in various types of turbojet engine, ...
A Westinghouse 24C-2 combustor was investigated at conditions simulating operation of the 24C Jet en...
An investigation was conducted in an altitude test chamber at the NACA Lewis laboratory to determine...
An altitude-test-chamber investigation was conducted to determine the operational and performance ch...
A brief investigation has been made of the performance of a single combustor of the TG-180 turboJet ...
An investigation was conducted in the Cleveland altitude wind tunnel to determine the operational ch...
Experimental investigation of engine dynamics and controls for 48-inch ramjet engine in free jet fac...
An investigation of turbojet-engine thrust augmentation by means of tail-pipe burning has been condu...
A preliminary evaluation was made of three types of combustor configurations in a 48-inch-diameter r...