Analysis indicates that this use of spoiler ailerons is feasible and desirable for normal emergency operatiion of airplanes. These speed brakes or glide-path controls would probably have small effect on wing pitching moments and should retain their rolling effectiveness.Ths report contains the results and discussion of an investigation of plug and retractable ailerons used as speed brakes or glide-path controls on an NACA 65-210 wing and an NACA 65₂-215 wing of aspect ratio 5.76 equipped with full-span slotted flaps. Incremental lift, drag, and pitching-moment data are presented for various flap conditions through a large-scale angle-or-attack range at Mach numbers from 0.13 to 0.71.NACA TN No. 1933."August 1949."Includes bibliographical re...
The increased use of split flaps for the dual purpose of reducing the landing speed and shortening t...
Ailerons having a beveled trailing edge and a blunt-nose overhang of 35 percent aileron chord on an ...
An investigation was conducted in a 300-mph 7- by 10- foot tunnel to obtain data for a slot spoiler ...
A wind-tunnel investigation was made to determine the characteristics of spoiler ailerons used as sp...
An analysis has been made of the lift control effectiveness of a 20-percent-chord plain trailing-edg...
A flight investigation was conducted to determine the lateral-control characteristics of retractable...
An analysis has been made of the lift control effectiveness of a 20-percent-chord plain trailing-edg...
An investigation has been made in the Langley 4- by 4-foot supersonic pressure tunnel at Mach number...
In te res t i n spoiler-typa ailerons has been intensif ied recently mainly because they give high r...
The failure of wing panels on a number of TBF-1 and TBM-1 airplanes in flight has prompted several i...
An investigation has been conducted in the Langley 19-foot pressure tunnel to determine the maximum ...
An investigation was made in the LMAL 7- by 10-foot tunnel of various modifications to the trailing ...
This paper presents the results of an investigation to determine the control-effectiveness character...
Flight measurements have been made to determine the characteristics of a pair of experimental ailero...
The increased use of split flaps for the dual purpose of reducing the landing speed and shortening t...
Ailerons having a beveled trailing edge and a blunt-nose overhang of 35 percent aileron chord on an ...
An investigation was conducted in a 300-mph 7- by 10- foot tunnel to obtain data for a slot spoiler ...
A wind-tunnel investigation was made to determine the characteristics of spoiler ailerons used as sp...
An analysis has been made of the lift control effectiveness of a 20-percent-chord plain trailing-edg...
A flight investigation was conducted to determine the lateral-control characteristics of retractable...
An analysis has been made of the lift control effectiveness of a 20-percent-chord plain trailing-edg...
An investigation has been made in the Langley 4- by 4-foot supersonic pressure tunnel at Mach number...
In te res t i n spoiler-typa ailerons has been intensif ied recently mainly because they give high r...
The failure of wing panels on a number of TBF-1 and TBM-1 airplanes in flight has prompted several i...
An investigation has been conducted in the Langley 19-foot pressure tunnel to determine the maximum ...
An investigation was made in the LMAL 7- by 10-foot tunnel of various modifications to the trailing ...
This paper presents the results of an investigation to determine the control-effectiveness character...
Flight measurements have been made to determine the characteristics of a pair of experimental ailero...
The increased use of split flaps for the dual purpose of reducing the landing speed and shortening t...
Ailerons having a beveled trailing edge and a blunt-nose overhang of 35 percent aileron chord on an ...
An investigation was conducted in a 300-mph 7- by 10- foot tunnel to obtain data for a slot spoiler ...