The paper deals with the experimental evaluation of the feasibility and effectiveness of active control of longitudinal vibration on a helicopter gearbox support strut. The aim is to test practical solutions for helicopter interior noise reduction using active control techniques. Very annoying components of cabin noise are associated with gearbox meshing tones. A preliminary transmissibility analysis of the vibration path between the gearbox and the helicopter fuselage showed the predominant contribution of the longitudinal vibration. Thus the experiments were arranged and performed on a strut under longitudinal disturbance conditions. The strut was connected with two end masses to roughly reproduce terminal impedances and equipped with a p...
Helicopter fuselage vibrations are of significant levels and produce a unique vibration problem. Red...
Although the acoustic comfort in helicopter cabins is not subject to European Recommendations regar...
The main objective of this research project is to study the feasibility and effectiveness of active ...
The paper deals with the experimental evaluation of the feasibility and effectiveness of active cont...
The paper presents the preliminary testing results of an active gearbox strut control system on a he...
A special periodic strut is developed to reduce the helicopter cabin noise in this paper. The strut ...
The paper presents some preliminary results of active control strategies aimed at reducing the trans...
In the framework of the European project FRIENDCOPTER, the Department of Aerospace Engineering of Po...
The high level vibration of helicopter flight can cause physiological damage to the aircrew and may ...
This paper presents the performance evaluation of a multi-axis active helicopter seat mount. By simu...
In this article, theoretical and the experimental studies are reported on the adaptive control of vi...
The increased need for lightweight structures in modern aerospace transport due to lower fuel consum...
Helicopter fuselage vibrations are of significant levels and produce a unique vibration problem. Red...
Although the acoustic comfort in helicopter cabins is not subject to European Recommendations regar...
The main objective of this research project is to study the feasibility and effectiveness of active ...
The paper deals with the experimental evaluation of the feasibility and effectiveness of active cont...
The paper presents the preliminary testing results of an active gearbox strut control system on a he...
A special periodic strut is developed to reduce the helicopter cabin noise in this paper. The strut ...
The paper presents some preliminary results of active control strategies aimed at reducing the trans...
In the framework of the European project FRIENDCOPTER, the Department of Aerospace Engineering of Po...
The high level vibration of helicopter flight can cause physiological damage to the aircrew and may ...
This paper presents the performance evaluation of a multi-axis active helicopter seat mount. By simu...
In this article, theoretical and the experimental studies are reported on the adaptive control of vi...
The increased need for lightweight structures in modern aerospace transport due to lower fuel consum...
Helicopter fuselage vibrations are of significant levels and produce a unique vibration problem. Red...
Although the acoustic comfort in helicopter cabins is not subject to European Recommendations regar...
The main objective of this research project is to study the feasibility and effectiveness of active ...