In this work, flutter behaviour of NACA 6409 is investigated using wind tunnel. The plunging and pitching oscillation of the wing is being observed to determine the dynamic instability point. The elastic axis will be manipulated in the experiment where the position of the elastic axis was varied at 25% 50% and 75% of the wing chord to determine the critical flutter speed. The effects on flutter speed at different elastic axis was discussed and analysed to explain the phenomenon. The method of designing and fabrication of the wing model and rig was presented step by step in the thesis. In the experiment the results show that the flutter speed for the elastic axis at 25% of the wing chord is the highest which is 17.84 m/s and follow by the ...
The results of the basic flutter theory originally devised in 1934 and published as NACA Technical R...
The aeroelastic behaviour of a wing oscillating in the heave and pitch degrees of freedom is examine...
A review is presented of the work done by other investigators on the effects of inertia couplings in...
This paper discusses the activities carried out during two years of a dedicated project to investiga...
This paper discusses the activities carried out during two years of a dedicated project to investiga...
This paper discusses the activities carried out during two years of a dedicated project to investiga...
This paper discusses the activities carried out during two years of a dedicated project to investiga...
This paper discusses the activities carried out during two years of a dedicated project to investiga...
A flexible mounting system has been developed for flutter tests with rigid wings in wind tunnel. The...
This thesis concerns the experimental analysis of the aerodynamics and aeroelasticity of oscillatin...
This paper discusses the generation and the testing of a wind tunnel model designed for the experime...
This paper discusses the generation and the testing of a wind tunnel model designed for the experime...
This paper discusses the generation and the testing of a wind tunnel model designed for the experime...
Low-speed flutter studies of a dynamically and elastically scaled model of a large multijet transpor...
This paper discusses the generation and the testing of a wind tunnel model designed for the experime...
The results of the basic flutter theory originally devised in 1934 and published as NACA Technical R...
The aeroelastic behaviour of a wing oscillating in the heave and pitch degrees of freedom is examine...
A review is presented of the work done by other investigators on the effects of inertia couplings in...
This paper discusses the activities carried out during two years of a dedicated project to investiga...
This paper discusses the activities carried out during two years of a dedicated project to investiga...
This paper discusses the activities carried out during two years of a dedicated project to investiga...
This paper discusses the activities carried out during two years of a dedicated project to investiga...
This paper discusses the activities carried out during two years of a dedicated project to investiga...
A flexible mounting system has been developed for flutter tests with rigid wings in wind tunnel. The...
This thesis concerns the experimental analysis of the aerodynamics and aeroelasticity of oscillatin...
This paper discusses the generation and the testing of a wind tunnel model designed for the experime...
This paper discusses the generation and the testing of a wind tunnel model designed for the experime...
This paper discusses the generation and the testing of a wind tunnel model designed for the experime...
Low-speed flutter studies of a dynamically and elastically scaled model of a large multijet transpor...
This paper discusses the generation and the testing of a wind tunnel model designed for the experime...
The results of the basic flutter theory originally devised in 1934 and published as NACA Technical R...
The aeroelastic behaviour of a wing oscillating in the heave and pitch degrees of freedom is examine...
A review is presented of the work done by other investigators on the effects of inertia couplings in...