The turbine-less jet engine, in its fourth iteration at California State University, Los Angeles, looks to improve the efficiency of jet propulsion. This iteration of the turbine-less jet engine focused on adding a combustor to the engine assembly to improve thrust performance. By testing various sized combustors with the turbine-less jet engine this gave insight on how they affect engine performance. It was found that while shorter combustors initially outperformed longer combustors, longer combustors are more fuel efficient in achieving thrust at higher fan power output. However, the turbine-less jet engine can still benefit from better designing and more extensive testing. Since the turbine-less jet engines performs best when the air flo...
Includes bibliographical references.A turbocharger designed to increase intake pressure of an intern...
The fuel efficiency of turbofan engines has improved significantly, hence reducing aviation's CO2 em...
A ram-jet engine with an experimental 48-inch-diameter combustor was investigated in a free-jet faci...
In a conventional turbojet and turbofan engine, fuel is burned in the main combustor before the heat...
A small turbine-less jet engine prototype has been developed at California State University, Los Ang...
The gas turbine propulsion system has been playing the most significant role in the evolution and de...
The gas turbine propulsion system has been playing the most significant role in the evolution and de...
The gas turbine propulsion system has been playing the most significant role in the evolution and de...
The gas turbine propulsion system has been playing the most significant role in the evolution and de...
The gas turbine propulsion system has been playing the most significant role in the evolution and de...
Presented herein is a comparative performance analysis of a novel turbofan engine with an auxiliary ...
This Ignite Project Proposal for Unmanned Aerial Vehicle (UAV) Propulsion Research is a continuation...
poster abstractThe gas turbine has been an enormously successful power plant for aircraft and marine...
Unmanned Aerial Vehicles are becoming more commonly used in today’s society, ranging anywhere from m...
Gas turbines are becoming increasingly used as power generators for a wide variety of applications a...
Includes bibliographical references.A turbocharger designed to increase intake pressure of an intern...
The fuel efficiency of turbofan engines has improved significantly, hence reducing aviation's CO2 em...
A ram-jet engine with an experimental 48-inch-diameter combustor was investigated in a free-jet faci...
In a conventional turbojet and turbofan engine, fuel is burned in the main combustor before the heat...
A small turbine-less jet engine prototype has been developed at California State University, Los Ang...
The gas turbine propulsion system has been playing the most significant role in the evolution and de...
The gas turbine propulsion system has been playing the most significant role in the evolution and de...
The gas turbine propulsion system has been playing the most significant role in the evolution and de...
The gas turbine propulsion system has been playing the most significant role in the evolution and de...
The gas turbine propulsion system has been playing the most significant role in the evolution and de...
Presented herein is a comparative performance analysis of a novel turbofan engine with an auxiliary ...
This Ignite Project Proposal for Unmanned Aerial Vehicle (UAV) Propulsion Research is a continuation...
poster abstractThe gas turbine has been an enormously successful power plant for aircraft and marine...
Unmanned Aerial Vehicles are becoming more commonly used in today’s society, ranging anywhere from m...
Gas turbines are becoming increasingly used as power generators for a wide variety of applications a...
Includes bibliographical references.A turbocharger designed to increase intake pressure of an intern...
The fuel efficiency of turbofan engines has improved significantly, hence reducing aviation's CO2 em...
A ram-jet engine with an experimental 48-inch-diameter combustor was investigated in a free-jet faci...