The effect of flight velocity on the jet noise and thrust of a 104-tube suppressor nozzle was investigated using an F-106B delta wing aircraft modified to carry two underwing nacelles each containing a turbojet engine. The nozzle was mounted behind one of the nacelles. Flight velocity had a large adverse effect on thrust and a small adverse effect on suppression when correlated with relative jet velocity. The clean airframe noise of the aircraft was measured at Mach 0.4 and was compared with that predicted from an empirical expression. The 83 db measured value was considerably below the predicted value
An investigation to determine the effect of forward speed on the exhaust noise from a conical ejecto...
A modified F-106B aircraft with underwing engine nacelles was flight tested to investigate airframe ...
Experimental acoustic data are presented to illustrate, at model scale, the effect of varying the no...
To determine flyover noise and thrust and to investigate whether flight velocity significantly affec...
At the relatively high takeoff speeds of supersonic transport aircraft, an important question concer...
Because of the relatively high takeoff speeds of supersonic transport aircraft, it is important to k...
Two spoke-type suppressor plug nozzles and a basic plug nozzle were tested for noise and thrust perf...
Because of the relatively high takeoff speeds of supersonic transport aircraft, it is important to k...
The effect of external air flowing across exhaust nozzles on the jet noise characteristics of supers...
It is important to know whether the relatively high takeoff speeds of supersonic transport aircraft ...
To establish a realistic lower limit for the noise level of advanced supersonic transport aircraft w...
Two aft underwing nacelles housing afterburning J85 engines were added to an F106 to study exhaust n...
Flight and wind tunnel noise tests were conducted using a J85 turbojet engine as a part of comprehen...
The results of a test program conducted in the NASA Ames 40- by 80-Foot Wind Tunnel to determine the...
Airframe installation effects on variable flap ejector nozzle of underwing engine nacell
An investigation to determine the effect of forward speed on the exhaust noise from a conical ejecto...
A modified F-106B aircraft with underwing engine nacelles was flight tested to investigate airframe ...
Experimental acoustic data are presented to illustrate, at model scale, the effect of varying the no...
To determine flyover noise and thrust and to investigate whether flight velocity significantly affec...
At the relatively high takeoff speeds of supersonic transport aircraft, an important question concer...
Because of the relatively high takeoff speeds of supersonic transport aircraft, it is important to k...
Two spoke-type suppressor plug nozzles and a basic plug nozzle were tested for noise and thrust perf...
Because of the relatively high takeoff speeds of supersonic transport aircraft, it is important to k...
The effect of external air flowing across exhaust nozzles on the jet noise characteristics of supers...
It is important to know whether the relatively high takeoff speeds of supersonic transport aircraft ...
To establish a realistic lower limit for the noise level of advanced supersonic transport aircraft w...
Two aft underwing nacelles housing afterburning J85 engines were added to an F106 to study exhaust n...
Flight and wind tunnel noise tests were conducted using a J85 turbojet engine as a part of comprehen...
The results of a test program conducted in the NASA Ames 40- by 80-Foot Wind Tunnel to determine the...
Airframe installation effects on variable flap ejector nozzle of underwing engine nacell
An investigation to determine the effect of forward speed on the exhaust noise from a conical ejecto...
A modified F-106B aircraft with underwing engine nacelles was flight tested to investigate airframe ...
Experimental acoustic data are presented to illustrate, at model scale, the effect of varying the no...