The relative aero-acoustic effectiveness of two core engine suppressors, a contractor-designed suppressor delivered with the Quiet Engine, and a NASA-designed suppressor was evaluated. The NASA suppressor was tested with and without a splitter making a total of three configurations being reported in addition to the baseline hardwall case. The aerodynamic results are presented in terms of tailpipe pressure loss, corrected net thrust, and corrected specific fuel consumption as functions of engine power setting. The acoustic results are divided into duct and far-field acoustic data. The NASA-designed core suppressor did the better job of suppressing aft end noise, but the splitter associated with it caused a significant engine performance pena...
An analysis procedure was developed for design of acoustically treated nacelles for high bypass turb...
A series of acoustic tests were conducted on the over the wing engine. These tests evaluated the ful...
Design considerations for integration of turbofan engine with reduced noise output in jet aircraf
The length of multiple-pure-tone (MPT) treatment required to reasonably suppress the MPT's produced ...
The acoustic investigation and evaluation of the C propulsion turbofan engine are discussed. The eng...
Efforts to develop an engine noise reduction technology suitable for use on subsonic and conventiona...
Acoustic performance tests were conducted with a three-ring inlet noise suppressor designed for a TF...
Full-scale low-tip-speed fans, a full-scale high-tip-speed fan, scale model versions of fans, and tw...
Acoustic and aerodynamic performance of six foot diameter fan for turbofan engines with noise suppre...
Acoustic measurements on jet engine intake system noise reduction suppressor cowling
Acoustic treatment was developed for jet engine turbine noise suppression. Acoustic impedance and du...
Application of noise reduction technology to design of propulsion system for subsonic civil transpor...
A lift fan exhaust suppression system to meet future VTOL aircraft noise goals was designed and test...
Acoustic treatment designs for the quiet clean short-haul experimental engines are defined. The proc...
Small scale model acoustic experiments were conducted to measure the noise produced in the flyover a...
An analysis procedure was developed for design of acoustically treated nacelles for high bypass turb...
A series of acoustic tests were conducted on the over the wing engine. These tests evaluated the ful...
Design considerations for integration of turbofan engine with reduced noise output in jet aircraf
The length of multiple-pure-tone (MPT) treatment required to reasonably suppress the MPT's produced ...
The acoustic investigation and evaluation of the C propulsion turbofan engine are discussed. The eng...
Efforts to develop an engine noise reduction technology suitable for use on subsonic and conventiona...
Acoustic performance tests were conducted with a three-ring inlet noise suppressor designed for a TF...
Full-scale low-tip-speed fans, a full-scale high-tip-speed fan, scale model versions of fans, and tw...
Acoustic and aerodynamic performance of six foot diameter fan for turbofan engines with noise suppre...
Acoustic measurements on jet engine intake system noise reduction suppressor cowling
Acoustic treatment was developed for jet engine turbine noise suppression. Acoustic impedance and du...
Application of noise reduction technology to design of propulsion system for subsonic civil transpor...
A lift fan exhaust suppression system to meet future VTOL aircraft noise goals was designed and test...
Acoustic treatment designs for the quiet clean short-haul experimental engines are defined. The proc...
Small scale model acoustic experiments were conducted to measure the noise produced in the flyover a...
An analysis procedure was developed for design of acoustically treated nacelles for high bypass turb...
A series of acoustic tests were conducted on the over the wing engine. These tests evaluated the ful...
Design considerations for integration of turbofan engine with reduced noise output in jet aircraf