In this thesis, a new approach to the selection of key fan design parameters is presented and a methodology to optimise engine operation for minimum take-off noise is developed. These techniques are applied to the detailed design of a fan system for the Cambridge-MIT Silent Aircraft Initiative engine to which ultra low noise is the principle design objective. Reduction of jet mixing noise is identified as being crucial to the design process leading to jet area at take-off having to be increased significantly compared to current trends. Whilst increasing the number of engines from two to three and optimisation of the departure profile reduced this area increase, the introduction of variable cycle technology is required in order to deliver lo...
Aircraft propulsion will continue to rely on gas turbine technology for the next decades to come. Th...
The current form of the Silent Aircraft is a blended wing design with the propulsion system embedded...
Design considerations for integration of turbofan engine with reduced noise output in jet aircraf
Meeting the Silent Aircraft Initiative (SAI) design goal during take-off drives the aircraft and eng...
A low-noise low-pressure ultra-high-bypass-ratio fan stage to be implemented in the next generation ...
The noise emitted by commercial aircraft is a major inhibitor of the growth of commercial air transp...
This paper presents a three-dimensional airframe design methodology for low noise emission and high ...
This paper discusses characteristic multi-disciplinary issues related to quiet short take-off and la...
The noise (unwanted sound) from fans of all sizes, operating in close proximity to people, can be a ...
The NASA Glenn Research Center recently completed an experimental study to reduce the jet noise from...
A propulsion system, comprising of a low pressure ratio fan stage with bypass and core section and a...
As aircraft noise is a major concern for residents living in the vicinity of airports, this thesis i...
Abstract Aircraft noise remains the key inhibitor of the growth of air transportation...
A propulsion system, comprising of a low pressure ratio fan stage with bypass and core section and a...
Among the various environmental concerns, the aircraft noise item has been constantly growing in imp...
Aircraft propulsion will continue to rely on gas turbine technology for the next decades to come. Th...
The current form of the Silent Aircraft is a blended wing design with the propulsion system embedded...
Design considerations for integration of turbofan engine with reduced noise output in jet aircraf
Meeting the Silent Aircraft Initiative (SAI) design goal during take-off drives the aircraft and eng...
A low-noise low-pressure ultra-high-bypass-ratio fan stage to be implemented in the next generation ...
The noise emitted by commercial aircraft is a major inhibitor of the growth of commercial air transp...
This paper presents a three-dimensional airframe design methodology for low noise emission and high ...
This paper discusses characteristic multi-disciplinary issues related to quiet short take-off and la...
The noise (unwanted sound) from fans of all sizes, operating in close proximity to people, can be a ...
The NASA Glenn Research Center recently completed an experimental study to reduce the jet noise from...
A propulsion system, comprising of a low pressure ratio fan stage with bypass and core section and a...
As aircraft noise is a major concern for residents living in the vicinity of airports, this thesis i...
Abstract Aircraft noise remains the key inhibitor of the growth of air transportation...
A propulsion system, comprising of a low pressure ratio fan stage with bypass and core section and a...
Among the various environmental concerns, the aircraft noise item has been constantly growing in imp...
Aircraft propulsion will continue to rely on gas turbine technology for the next decades to come. Th...
The current form of the Silent Aircraft is a blended wing design with the propulsion system embedded...
Design considerations for integration of turbofan engine with reduced noise output in jet aircraf