In this chapter, the origin and remediation of an important sliding in the overconsolidated Boom Clay in Kruibeke (Belgium) is discussed. Local and environmental factors caused an unstable slope about 30 m deep, A larger sensitivity to erosion resulted finally in the instability of the slope. Because of the formation of fine cracks in the soil there was a possibility for the water to penetrate in the clay close to the surface, resulting in the presence of higher water pressures. Also, the presence of the excavator on top of the slope during exploitation had an important impact on the stress state of the soil. Both an analytical and numerical approach were used to estimate the factor of safety. Because of the change of the soil characteristi...
A study was made to investigate the potential errors in stability assessments when using conventiona...
There are several factors that effect the level security of a slope. Such as the condition of a slop...
An investigation has been conducted to gain a better understanding of the drained residual and fully...
In this chapter, the origin and remediation of an important sliding in the overconsolidated Boom Cla...
In this chapter, the origin and remediation of an important sliding in the overconsolidated Boom Cla...
Many natural and man-made slopes close to buildings or infrastructure do not demonstrate sufficient ...
Mechanical weakening of shallow sloping covers is a typical phenomenon occurring in overconsolidated...
A brief state-of-the-art review of the effects of water on slope stability and the techniques for an...
Mechanical weakening of shallow sloping covers is a typical phenomenon occurring in overconsolidated...
Many natural and man-made slopes close to buildings or infrastructure do not demonstrate sufficient ...
Some slope instability problems exist in Ankara clay along E90 highway. The purpose of this paper is...
The behaviour of an instrumented unstable slope in a profile of weathered overconsolidated clay has ...
This paper describes some of the main results of physical modelling tests performed on retaining str...
This paper presents results of stability and deformation analysis of several failed embankment case ...
International audienceA future development site of a housing estate, an abandoned-brick yard with cl...
A study was made to investigate the potential errors in stability assessments when using conventiona...
There are several factors that effect the level security of a slope. Such as the condition of a slop...
An investigation has been conducted to gain a better understanding of the drained residual and fully...
In this chapter, the origin and remediation of an important sliding in the overconsolidated Boom Cla...
In this chapter, the origin and remediation of an important sliding in the overconsolidated Boom Cla...
Many natural and man-made slopes close to buildings or infrastructure do not demonstrate sufficient ...
Mechanical weakening of shallow sloping covers is a typical phenomenon occurring in overconsolidated...
A brief state-of-the-art review of the effects of water on slope stability and the techniques for an...
Mechanical weakening of shallow sloping covers is a typical phenomenon occurring in overconsolidated...
Many natural and man-made slopes close to buildings or infrastructure do not demonstrate sufficient ...
Some slope instability problems exist in Ankara clay along E90 highway. The purpose of this paper is...
The behaviour of an instrumented unstable slope in a profile of weathered overconsolidated clay has ...
This paper describes some of the main results of physical modelling tests performed on retaining str...
This paper presents results of stability and deformation analysis of several failed embankment case ...
International audienceA future development site of a housing estate, an abandoned-brick yard with cl...
A study was made to investigate the potential errors in stability assessments when using conventiona...
There are several factors that effect the level security of a slope. Such as the condition of a slop...
An investigation has been conducted to gain a better understanding of the drained residual and fully...