ABSTRACT The results of an experimental investigation of the flow in a high-speed annular compressor cascade with a hub tip clearance gap and a rotating hub wall are presented. 3-1) flow measuranents are conducted by means of WA and five hole probes. Detailed flow field data are presented at successive axial planes in a blade passage. Blade surface pressure distributions are also used, to support the interpretation of the in-passage measuremans. The features of the clearance flow are captured and discussed Results are shown for two sizes of the tip clearance gap, while relative wall motion is present_ The features of the flow revealed by the present investigation are compared to existing information from low speed studies and it is conclude...
An experimental investigation on casing treatments in a one-stage transonic compressor is presented....
An effective method to improve gas turbine propulsive efficiency is to increase the bypass ratio. Wi...
The primary focus of this paper is to investigate how a rotor’s unsteady tip clearance flow structur...
The focus of this work was to characterize the fundamental flow physics and the overall performance ...
The tip clearance flow of industrial axial compressor rotors has a significant impact on compressor ...
This paper reports on an experimental study of the nature of the tip clearance flow in a moderately ...
The effect of rotor tip clearances in turbomachinery applications has been a primary research intere...
This paper presents an experimental investigation of effects of axially non-uniform tip clearances o...
Large tip clearances typically in the region of 6% exist in the high pressure (HP) stages of compres...
Large tip clearances typically in the region of six percent exist in the high pressure stages of com...
Large tip clearances typically in the region of six percent exist in the high pressure stages of com...
An analytical and experimental study of the performance changes and flow effects of rotor tip cleara...
The tip clearance flow within industrial axial compressor rows has a significant impact on compresso...
Experimental and computational techniques are used to investigate tip clearance flows in a transonic...
Large tip clearances in the region of six percent span exist in the high pressure stages of compress...
An experimental investigation on casing treatments in a one-stage transonic compressor is presented....
An effective method to improve gas turbine propulsive efficiency is to increase the bypass ratio. Wi...
The primary focus of this paper is to investigate how a rotor’s unsteady tip clearance flow structur...
The focus of this work was to characterize the fundamental flow physics and the overall performance ...
The tip clearance flow of industrial axial compressor rotors has a significant impact on compressor ...
This paper reports on an experimental study of the nature of the tip clearance flow in a moderately ...
The effect of rotor tip clearances in turbomachinery applications has been a primary research intere...
This paper presents an experimental investigation of effects of axially non-uniform tip clearances o...
Large tip clearances typically in the region of 6% exist in the high pressure (HP) stages of compres...
Large tip clearances typically in the region of six percent exist in the high pressure stages of com...
Large tip clearances typically in the region of six percent exist in the high pressure stages of com...
An analytical and experimental study of the performance changes and flow effects of rotor tip cleara...
The tip clearance flow within industrial axial compressor rows has a significant impact on compresso...
Experimental and computational techniques are used to investigate tip clearance flows in a transonic...
Large tip clearances in the region of six percent span exist in the high pressure stages of compress...
An experimental investigation on casing treatments in a one-stage transonic compressor is presented....
An effective method to improve gas turbine propulsive efficiency is to increase the bypass ratio. Wi...
The primary focus of this paper is to investigate how a rotor’s unsteady tip clearance flow structur...