Presented at the International Gas Turbine and Aeroengine Congress and Exposition Orlando, FL June 3-6, 1991This paper describes the effect of tip clearance changes on the pressure at the case wall of a second stage rotor. Wall shear distributions under the rotor tip are also presented. The results show low pressure areas extending along the rotor suction side but lying away from the blade. Pressure contours indicate the tangential loading at the tip is lower than predicted by two dimensional calculations, however, the predicted loading is observed between the lowest pressure’s path in the passage and the blade pressure side. The results suggest a viscous or shearing layer, due to blade-to-wall relative motion, is generated on the blade si...
A 30-inch tip-diameter axial-flow compressor stage was investigated with and without rotor to determ...
This thesis investigates over tip leakage where the tip clearance is large. In the high pressure sta...
Total turbine blade performance was investigated while changing the blade tip clearance in three way...
The article of record as published may be found at http://dx.doi.org/10.2514/3.24129Presented as Pap...
An analytical and experimental study of the performance changes and flow effects of rotor tip cleara...
Thesis: S.M., Massachusetts Institute of Technology, Department of Aeronautics and Astronautics, 201...
The effect of rotor tip clearances in turbomachinery applications has been a primary research intere...
In the present study, the numerical analysis of blade tip geometry effect on the performance of a si...
Thesis (M.Sc.)-University of Natal, Durban, 1989.On unshrouded axial flow turbine rotors, the tip cl...
International audienceMultistage compressor is the most important constituent of gas turbines used i...
Experimental and computational techniques are used to investigate tip clearance flows in a transonic...
In the current study, the influence of blade tip clearance in different stages of a three-stage comp...
The tip clearance flow of industrial axial compressor rotors has a significant impact on compressor ...
The focus of this work was to characterize the fundamental flow physics and the overall performance ...
The tip clearance flow within industrial axial compressor rows has a significant impact on compresso...
A 30-inch tip-diameter axial-flow compressor stage was investigated with and without rotor to determ...
This thesis investigates over tip leakage where the tip clearance is large. In the high pressure sta...
Total turbine blade performance was investigated while changing the blade tip clearance in three way...
The article of record as published may be found at http://dx.doi.org/10.2514/3.24129Presented as Pap...
An analytical and experimental study of the performance changes and flow effects of rotor tip cleara...
Thesis: S.M., Massachusetts Institute of Technology, Department of Aeronautics and Astronautics, 201...
The effect of rotor tip clearances in turbomachinery applications has been a primary research intere...
In the present study, the numerical analysis of blade tip geometry effect on the performance of a si...
Thesis (M.Sc.)-University of Natal, Durban, 1989.On unshrouded axial flow turbine rotors, the tip cl...
International audienceMultistage compressor is the most important constituent of gas turbines used i...
Experimental and computational techniques are used to investigate tip clearance flows in a transonic...
In the current study, the influence of blade tip clearance in different stages of a three-stage comp...
The tip clearance flow of industrial axial compressor rotors has a significant impact on compressor ...
The focus of this work was to characterize the fundamental flow physics and the overall performance ...
The tip clearance flow within industrial axial compressor rows has a significant impact on compresso...
A 30-inch tip-diameter axial-flow compressor stage was investigated with and without rotor to determ...
This thesis investigates over tip leakage where the tip clearance is large. In the high pressure sta...
Total turbine blade performance was investigated while changing the blade tip clearance in three way...