Failed brake pads of a particular type of aircraft were analyzed. The friction material and the bonding between the back plate and the friction material were found satisfactory. No metallurgical abnormalities were found responsible for the failure. Analysis shows that the chipping off of the friction material occurred due to excessive load on the pad as a result of jamming of the brake. Measurements showed that the thickness of the pads was in the range 0.13 – 0.14 inch against the minimum specified value of 0.193 inch. Whether or not the use of worn out pads with less thickness was responsible for the jamming of the brake needs to be examined
A fractured main undercarriage fitting of an aircraft was analyzed. Analysis revealed that there was...
A failed wheel nut belonging to an aircraft was sent to the laboratory for investigation. Examinati...
Evidences suggest that the indentation marks on the rollers and the cracks on the bearing cup were r...
Failed brake pads of a particular type of aircraft were analyzed. The friction material and the bond...
This paper presents the failure analysis of a broken main wheel brake assembly of a Royal Malaysian ...
This paper presents the results of a failure analysis investigation conducted in the braking compone...
Due to post fracture damage, the fractographic features of the rivet surfaces were completely oblite...
The major concern in the aviation industry is the flight safety. Although great effort has been put ...
The main fitting subassembly of main landing gear of an aircraft was sent to the laboratory for ana...
Evidences suggest that the torque plate has failed by stress corrosion cracking (SCC). Microstructur...
A set of damaged bearing shells along with a set of unused bearing shells of an aeroengine were sent...
Damaged parts of bearings of a wheel hub of an aircraft were sent to the laboratory for analysis. Th...
On April 09, 2005 at approximately 16.00 Hrs, the aircraft force landed in a cultivatable field foll...
Failed plate assemblies from two aircrafts were analyzed. Fractographic study showed that in both th...
The aircraft met with an incident on March 23, 2006. On strip examination of the engine, one of the ...
A fractured main undercarriage fitting of an aircraft was analyzed. Analysis revealed that there was...
A failed wheel nut belonging to an aircraft was sent to the laboratory for investigation. Examinati...
Evidences suggest that the indentation marks on the rollers and the cracks on the bearing cup were r...
Failed brake pads of a particular type of aircraft were analyzed. The friction material and the bond...
This paper presents the failure analysis of a broken main wheel brake assembly of a Royal Malaysian ...
This paper presents the results of a failure analysis investigation conducted in the braking compone...
Due to post fracture damage, the fractographic features of the rivet surfaces were completely oblite...
The major concern in the aviation industry is the flight safety. Although great effort has been put ...
The main fitting subassembly of main landing gear of an aircraft was sent to the laboratory for ana...
Evidences suggest that the torque plate has failed by stress corrosion cracking (SCC). Microstructur...
A set of damaged bearing shells along with a set of unused bearing shells of an aeroengine were sent...
Damaged parts of bearings of a wheel hub of an aircraft were sent to the laboratory for analysis. Th...
On April 09, 2005 at approximately 16.00 Hrs, the aircraft force landed in a cultivatable field foll...
Failed plate assemblies from two aircrafts were analyzed. Fractographic study showed that in both th...
The aircraft met with an incident on March 23, 2006. On strip examination of the engine, one of the ...
A fractured main undercarriage fitting of an aircraft was analyzed. Analysis revealed that there was...
A failed wheel nut belonging to an aircraft was sent to the laboratory for investigation. Examinati...
Evidences suggest that the indentation marks on the rollers and the cracks on the bearing cup were r...