Wind-tunnel tests were carried out to evaluate the performance of the Computational Fluid Dynamics (CFD)-based air-intake duct shape optimisation of the European platform tiltrotor ERICA. A 1/2.5 scale model including the nacelle, the external portion of the wing and two interchangeable internal ducts reproducing the baseline and optimised shape were manufactered to be tested in the large wind tunnel of Politecnico di Milano. Moreover, tests were carried out with the model equipped with rotating blade stubs. The comprehensive experimental campaign included tests reproducing different forward flight conditions of the aircraft including cruise and conversion phases. The evaluation of the internal duct performance was carried out by measuring ...
Aerodynamic characteristics of helicopter engine side air intakes are investigated. The experimental...
In the framework of the European JTI CleanSky GRC2 project devoted to drag reduction of airframe and...
The aerodynamic re-design and characterization of the Erica tilt-rotor aircraft, carried out by some...
Wind-tunnel tests were carried out to evaluate the performance of the Computational Fluid Dynamics (...
The present paper describes the experimental activity carried out at Politecnico di Milano large win...
The present paper describes the experimental set up of the wind tunnel activity to assess the effect...
A wide aerodynamic test campaign has been carried out on the tiltrotor aircraft ERICA at the Large W...
The purpose of this study is to to assess the improvement of the aerodynamic characteristics of tilt...
The results of a CFD-based optimization over a 1/8-scaled model of the ERICA tiltrotor fuselage are ...
A comparison of experimental data with several numerical predictions of the aerodynamic loads on the...
It is investigated whether a nonrotating lifting fan remaining uncovered during cruise flight, as op...
An aerodynamic study on efficiency improvement of a wing embedded lifting fan with a diameter of 0.3...
The always growing interest that rotorcraft manufacturers on reducing the environmental impact of th...
International audienceWind-tunnel tests of a heavy-class helicopter model were carried out to evalua...
Aerodynamic characteristics of helicopter engine side air intakes are investigated. The experimental...
In the framework of the European JTI CleanSky GRC2 project devoted to drag reduction of airframe and...
The aerodynamic re-design and characterization of the Erica tilt-rotor aircraft, carried out by some...
Wind-tunnel tests were carried out to evaluate the performance of the Computational Fluid Dynamics (...
The present paper describes the experimental activity carried out at Politecnico di Milano large win...
The present paper describes the experimental set up of the wind tunnel activity to assess the effect...
A wide aerodynamic test campaign has been carried out on the tiltrotor aircraft ERICA at the Large W...
The purpose of this study is to to assess the improvement of the aerodynamic characteristics of tilt...
The results of a CFD-based optimization over a 1/8-scaled model of the ERICA tiltrotor fuselage are ...
A comparison of experimental data with several numerical predictions of the aerodynamic loads on the...
It is investigated whether a nonrotating lifting fan remaining uncovered during cruise flight, as op...
An aerodynamic study on efficiency improvement of a wing embedded lifting fan with a diameter of 0.3...
The always growing interest that rotorcraft manufacturers on reducing the environmental impact of th...
International audienceWind-tunnel tests of a heavy-class helicopter model were carried out to evalua...
Aerodynamic characteristics of helicopter engine side air intakes are investigated. The experimental...
In the framework of the European JTI CleanSky GRC2 project devoted to drag reduction of airframe and...
The aerodynamic re-design and characterization of the Erica tilt-rotor aircraft, carried out by some...