The aerodynamic performance and associated flow physics of box wings at low Reynolds number as a function of variation in gap and stagger were experimentally investigated. To reduce the experimental parametric space for flow physics investigations, a set of cases were strategically selected based on results from a vortex lattice study. The effects of gap and stagger appear to be the dominating effects for biplanes joined at the tips by endplates; Gap was found to have the greatest effect and stagger the second greatest effect on the aerodynamic performance of a biplane with endplates using both inviscid computational and experimental techniques. Efforts to discern the optimal balance between reduced lift induced drag due to the presence of ...
Wings on airplanes and Unmanned Aerial Vehicles (UAVs) have a very important role in the formation o...
This work outlines the different aerodynamic aspects of box-wing design i.e. an unconventional air...
This conceptual design study of a 150-seat short-rang aircraft was undertaken to investigate whether...
Modern flow diagnostics applied to a very old aerodynamic problem produced a number of intriguing ne...
Modern flow diagnostics applied to a very old aerodynamic problem has produced a number of intriguin...
Modern flow diagnostics applied to a very old aerodynamic problem has produced a number of intriguin...
A parametric investigation has been conducted on a new multiple lifting surface configuration. This ...
A number of methods have been proposed to estimate the lift of a biplane based mostly on potential f...
A parametric investigation has been conducted on a new multiple lifting surface configuration. This ...
[EN] The main objective of this project is to study the aerodynamic interaction between the wings i...
A computational fluid dynamics study of the influence of wing span has been conducted for an inverte...
Numerical analysis for the aerodynamic characteristics of the WIG (wing-in ground effect) craft with...
ABSTRACTWe investigated the aerodynamic characteristics of a three-dimensional (3D) wing with an end...
The purpose of this investigation was to study the effect of improving the aerodynamic characteristi...
This report will summarize the work performed to better understand the aerodynamics and potential be...
Wings on airplanes and Unmanned Aerial Vehicles (UAVs) have a very important role in the formation o...
This work outlines the different aerodynamic aspects of box-wing design i.e. an unconventional air...
This conceptual design study of a 150-seat short-rang aircraft was undertaken to investigate whether...
Modern flow diagnostics applied to a very old aerodynamic problem produced a number of intriguing ne...
Modern flow diagnostics applied to a very old aerodynamic problem has produced a number of intriguin...
Modern flow diagnostics applied to a very old aerodynamic problem has produced a number of intriguin...
A parametric investigation has been conducted on a new multiple lifting surface configuration. This ...
A number of methods have been proposed to estimate the lift of a biplane based mostly on potential f...
A parametric investigation has been conducted on a new multiple lifting surface configuration. This ...
[EN] The main objective of this project is to study the aerodynamic interaction between the wings i...
A computational fluid dynamics study of the influence of wing span has been conducted for an inverte...
Numerical analysis for the aerodynamic characteristics of the WIG (wing-in ground effect) craft with...
ABSTRACTWe investigated the aerodynamic characteristics of a three-dimensional (3D) wing with an end...
The purpose of this investigation was to study the effect of improving the aerodynamic characteristi...
This report will summarize the work performed to better understand the aerodynamics and potential be...
Wings on airplanes and Unmanned Aerial Vehicles (UAVs) have a very important role in the formation o...
This work outlines the different aerodynamic aspects of box-wing design i.e. an unconventional air...
This conceptual design study of a 150-seat short-rang aircraft was undertaken to investigate whether...