Three Ti-6Al-4V bolts from mid-life jet aircraft failed during service operation. Each of the failed bolts were installed on a landing gear component. Metallurgical failure analysis indicated that the fracture mechanism is low temperature creep, possibly resulting from a sustained tension load over a long time. Visual inspection revealed ductile fracture morphology with no macroscopic deformation or corrosion. For all bolts fracture occurred close to the root at the first pitches of the thread. Scanning Electron Microscope (SEM) analysis revealed dimple morphologies with micro-void coalescence. Energy Dispersive X-Ray (EDX) analysis did not reveal any material deficiency that would have precipitated failure
Two fractured bolts belonging to an aircraft engine removal ground equipment were brought to the lab...
Two fractured bolts belonging to an aircraft engine removal ground equipment were brought to the lab...
A failed jack attachment bolt belonging to an aircraft was sent to the laboratory for investigation....
Three Ti-6Al-4V bolts from mid-life jet aircraft failed during service operation. Each of the failed...
Four failed bolts used in an aircraft were sent to the laboratory for analysis. Examination revealed...
Failed shear bolts used in the PTO shaft of an aircraft were analyzed. Examination showed that two o...
Four failed bolts used in an aircraft were sent to the laboratory for analysis. Examination revealed...
Two fractured main landing attachment bolts from an aircraft were sent to the laboratory for analysi...
Two fractured main landing attachment bolts from an aircraft were sent to the laboratory for analysi...
A few fractured bolts recovered from an in flight incident of an aircraft were received for analysi...
A few fractured bolts recovered from an in flight incident of an aircraft were received for analysi...
Failed bolts of main undercarriage torque link of an aircraft were analyzed. Examination did not rev...
Failed bolts of main undercarriage torque link of an aircraft were analyzed. Examination did not rev...
Nickel based superalloy Nimonic 80A is commonly used as high temperature bolting material in industr...
Two fractured bolts belonging to an aircraft engine removal ground equipment were brought to the lab...
Two fractured bolts belonging to an aircraft engine removal ground equipment were brought to the lab...
Two fractured bolts belonging to an aircraft engine removal ground equipment were brought to the lab...
A failed jack attachment bolt belonging to an aircraft was sent to the laboratory for investigation....
Three Ti-6Al-4V bolts from mid-life jet aircraft failed during service operation. Each of the failed...
Four failed bolts used in an aircraft were sent to the laboratory for analysis. Examination revealed...
Failed shear bolts used in the PTO shaft of an aircraft were analyzed. Examination showed that two o...
Four failed bolts used in an aircraft were sent to the laboratory for analysis. Examination revealed...
Two fractured main landing attachment bolts from an aircraft were sent to the laboratory for analysi...
Two fractured main landing attachment bolts from an aircraft were sent to the laboratory for analysi...
A few fractured bolts recovered from an in flight incident of an aircraft were received for analysi...
A few fractured bolts recovered from an in flight incident of an aircraft were received for analysi...
Failed bolts of main undercarriage torque link of an aircraft were analyzed. Examination did not rev...
Failed bolts of main undercarriage torque link of an aircraft were analyzed. Examination did not rev...
Nickel based superalloy Nimonic 80A is commonly used as high temperature bolting material in industr...
Two fractured bolts belonging to an aircraft engine removal ground equipment were brought to the lab...
Two fractured bolts belonging to an aircraft engine removal ground equipment were brought to the lab...
Two fractured bolts belonging to an aircraft engine removal ground equipment were brought to the lab...
A failed jack attachment bolt belonging to an aircraft was sent to the laboratory for investigation....