A new BWB concept aircraft was developed to meet the ACARE 2020 vision, NACRE-FW1. A patented feedforward controller was designed earlier at EADS Innovation Works to alleviate the gust loading, the controller was robust over various gust lengths and mass cases. The feedforward controller performed extremely well in reducing wing root moments for gusts longer than 60.9 meter, but the controller deteriorated the original aircraft performance by giving rise to the wing root moments for gust lengths shorter than 60.9 meter. This caused significant damage to the aircraft and affected the sizing issues of the wing root joints. This paper focuses on designing an additional robust control loop which would work together with patented Feedforward con...
Copyright © 2014 Elisa Capello et al. This is an open access article distributed under the Creative ...
The constant growth in air traffic has led to the necessity of developing new solutions to face the ...
The objective of this paper is the implementation and validation of an adaptive controller for aircr...
A new BWB concept aircraft was developed to meet the ACARE 2020 vision, NACRE-FW1. A patented feedfo...
The effects of gusts and turbulence do not only affect adversely the passenger comfort but also crea...
An active gust load alleviation (GLA) system offers great potential for weight savings in aircraft d...
Most of the gust load alleviation systems (GLAS) of currently-operational aircraft are of feedback-o...
The potential advantages of Blended Wing Body (BWB) aircraft in terms of fuel efficiency are opposed...
This paper presents a novel active gust load alleviation approach within a multi-objective flight co...
This paper presents a novel active gust load alleviation approach within a multi-objective flight co...
The master thesis work done by the author encompasses the design of a robust feed-forward controlle...
Gust alleviation is of great significance for improving aircraft ride quality and reducing gust load...
The design and assessment of a two degree of freedom gust load alleviation control system for a busi...
In this paper, a gust load alleviation system based on model-predictive control is developed for a v...
Turbulence and gusts are causing variations of the aerodynamic forces and moments that are applied t...
Copyright © 2014 Elisa Capello et al. This is an open access article distributed under the Creative ...
The constant growth in air traffic has led to the necessity of developing new solutions to face the ...
The objective of this paper is the implementation and validation of an adaptive controller for aircr...
A new BWB concept aircraft was developed to meet the ACARE 2020 vision, NACRE-FW1. A patented feedfo...
The effects of gusts and turbulence do not only affect adversely the passenger comfort but also crea...
An active gust load alleviation (GLA) system offers great potential for weight savings in aircraft d...
Most of the gust load alleviation systems (GLAS) of currently-operational aircraft are of feedback-o...
The potential advantages of Blended Wing Body (BWB) aircraft in terms of fuel efficiency are opposed...
This paper presents a novel active gust load alleviation approach within a multi-objective flight co...
This paper presents a novel active gust load alleviation approach within a multi-objective flight co...
The master thesis work done by the author encompasses the design of a robust feed-forward controlle...
Gust alleviation is of great significance for improving aircraft ride quality and reducing gust load...
The design and assessment of a two degree of freedom gust load alleviation control system for a busi...
In this paper, a gust load alleviation system based on model-predictive control is developed for a v...
Turbulence and gusts are causing variations of the aerodynamic forces and moments that are applied t...
Copyright © 2014 Elisa Capello et al. This is an open access article distributed under the Creative ...
The constant growth in air traffic has led to the necessity of developing new solutions to face the ...
The objective of this paper is the implementation and validation of an adaptive controller for aircr...