The mounting lug of the MGB housing of a helicopter has failed by fatigue. With the available evidences, it was not possible to establish the exact cause of the failure. Analysis shows that the fatigue crack initiation was due to one or more of the following reasons: (a) ovality in the lug bore and/or bush, (b) excessive rotational torque on the MGB housing, and (c) improper fitment. No metallurgical abnormalities were responsible for the failure. The microstructure and chemical composition of the housing material were found to conform to RZ-5 specification
A broken tail gearbox (TGB) housing and failed pitch link assemblies of a helicopter were sent to th...
All the three TGB housings had fatigue crack at the fillet of the lug fusing area with the temperatu...
All the three TGB housings had fatigue crack at the fillet of the lug fusing area with the temperatu...
The mounting lug of the MGB housing of a helicopter has failed by fatigue. With the available eviden...
A fractured MGB housing and a cracked TGB housing belonging to a helicopter were forwarded to the la...
A fractured MGB housing and a cracked TGB housing belonging to a helicopter were forwarded to the la...
The MGB housing of a helicopter had cracked by fatigue. The fatigue crack had initiated at the radiu...
The MGB housing of a helicopter had cracked by fatigue. The fatigue crack had initiated at the radiu...
The TGB housing had a 14 mm long fatigue crack at the fillet of the lug fusing area of one of the mo...
The TGB housing had a 14 mm long fatigue crack at the fillet of the lug fusing area of one of the mo...
The TGB housing had a 14 mm long fatigue crack at the fillet of the lug fusing area of one of the mo...
Two cracked Main Gear-Box (MGB) housings of a particular type of helicopter were referred to the lab...
A failed Tail Gear Box (TGB) housing of a helicopter was analyzed. Analysis showed that the gearbox ...
A failed Tail Gear Box (TGB) housing of a helicopter was analyzed. Analysis showed that the gearbox ...
A broken tail gearbox (TGB) housing and failed pitch link assemblies of a helicopter were sent to th...
A broken tail gearbox (TGB) housing and failed pitch link assemblies of a helicopter were sent to th...
All the three TGB housings had fatigue crack at the fillet of the lug fusing area with the temperatu...
All the three TGB housings had fatigue crack at the fillet of the lug fusing area with the temperatu...
The mounting lug of the MGB housing of a helicopter has failed by fatigue. With the available eviden...
A fractured MGB housing and a cracked TGB housing belonging to a helicopter were forwarded to the la...
A fractured MGB housing and a cracked TGB housing belonging to a helicopter were forwarded to the la...
The MGB housing of a helicopter had cracked by fatigue. The fatigue crack had initiated at the radiu...
The MGB housing of a helicopter had cracked by fatigue. The fatigue crack had initiated at the radiu...
The TGB housing had a 14 mm long fatigue crack at the fillet of the lug fusing area of one of the mo...
The TGB housing had a 14 mm long fatigue crack at the fillet of the lug fusing area of one of the mo...
The TGB housing had a 14 mm long fatigue crack at the fillet of the lug fusing area of one of the mo...
Two cracked Main Gear-Box (MGB) housings of a particular type of helicopter were referred to the lab...
A failed Tail Gear Box (TGB) housing of a helicopter was analyzed. Analysis showed that the gearbox ...
A failed Tail Gear Box (TGB) housing of a helicopter was analyzed. Analysis showed that the gearbox ...
A broken tail gearbox (TGB) housing and failed pitch link assemblies of a helicopter were sent to th...
A broken tail gearbox (TGB) housing and failed pitch link assemblies of a helicopter were sent to th...
All the three TGB housings had fatigue crack at the fillet of the lug fusing area with the temperatu...
All the three TGB housings had fatigue crack at the fillet of the lug fusing area with the temperatu...