A cracked engine mount of an aircraft was sent to the laboratory to analyze the cause of failure. Dye penetrant test indicated a crack at one of the weld joints. Investigation revealed this crack to be a fatigue crack. The fatigue crack had initiated at the weld – parent metal interface and propagated circumferentially about 12 mm. Microstructural study showed martensitic structure in the heat affected zone (HAZ). This was further corroborated by high hardness in this region. A section of the tube close to the HAZ was found to have low hardness (170-210 HV). This indicates improper heat treatment of the weld joint. It appears most probable that the abnormal microstructure in the HAZ and the low hardness of the tube adjacent to HAZ were res...
The fractured HPTR disc belonging to an aeroengine retrieved from the wreckage of an aircraft was in...
A failed main wheel hub of an aircraft was forwarded to the laboratory for analysis. Examination rev...
The analysis of multiple cracks in a heat exchanger tubeplate at a petrochemical plant led to experi...
A cracked engine mount of an aircraft was sent to the laboratory to analyze the cause of failure. Dy...
A failed engine mount frame of an aircraft was sent to the laboratory for investigation. The engine ...
The cooling tubes of both the aircraft have failed by fatigue. Fatigue cracks were found to have in...
A prematurely fractured main wheel hub of an aircraft was sent to the laboratory for investigation. ...
A prematurely fractured main wheel hub of an aircraft was sent to the laboratory for investigation. ...
The cooling tubes of both the aircraft have failed by fatigue. Fatigue cracks were found to have in...
A few fractured bolts recovered from an in flight incident of an aircraft were received for analysi...
Four failed components of an aeroengine were sent to the laboratory for determining the modes of fra...
A few fractured bolts recovered from an in flight incident of an aircraft were received for analysi...
The wheel hub in question has failed by fatigue. Three fatigue cracks were identified and all of the...
A fractured MGB housing and a cracked TGB housing belonging to a helicopter were forwarded to the la...
A fractured MGB housing and a cracked TGB housing belonging to a helicopter were forwarded to the la...
The fractured HPTR disc belonging to an aeroengine retrieved from the wreckage of an aircraft was in...
A failed main wheel hub of an aircraft was forwarded to the laboratory for analysis. Examination rev...
The analysis of multiple cracks in a heat exchanger tubeplate at a petrochemical plant led to experi...
A cracked engine mount of an aircraft was sent to the laboratory to analyze the cause of failure. Dy...
A failed engine mount frame of an aircraft was sent to the laboratory for investigation. The engine ...
The cooling tubes of both the aircraft have failed by fatigue. Fatigue cracks were found to have in...
A prematurely fractured main wheel hub of an aircraft was sent to the laboratory for investigation. ...
A prematurely fractured main wheel hub of an aircraft was sent to the laboratory for investigation. ...
The cooling tubes of both the aircraft have failed by fatigue. Fatigue cracks were found to have in...
A few fractured bolts recovered from an in flight incident of an aircraft were received for analysi...
Four failed components of an aeroengine were sent to the laboratory for determining the modes of fra...
A few fractured bolts recovered from an in flight incident of an aircraft were received for analysi...
The wheel hub in question has failed by fatigue. Three fatigue cracks were identified and all of the...
A fractured MGB housing and a cracked TGB housing belonging to a helicopter were forwarded to the la...
A fractured MGB housing and a cracked TGB housing belonging to a helicopter were forwarded to the la...
The fractured HPTR disc belonging to an aeroengine retrieved from the wreckage of an aircraft was in...
A failed main wheel hub of an aircraft was forwarded to the laboratory for analysis. Examination rev...
The analysis of multiple cracks in a heat exchanger tubeplate at a petrochemical plant led to experi...