A few fractured bolts recovered from an in flight incident of an aircraft were received for analysis. Examination revealed that all the bolts failed by fatigue. Fatigue cracks were found to have initiated at the thread roots of the bolts in all the cases and propagated progressively to over more than 90% of the cross section before culminating in overload failure. From the nature of striations, fatigue appears to be of high cycle – low stress type and vibration appears to be the most probable causative factor. Since the details of the bolts were not made available, it was not possible to examine whether or not the bolts meet the specification
A cracked engine mount of an aircraft was sent to the laboratory to analyze the cause of failure. Dy...
The wheel hub in question has failed by fatigue. Three fatigue cracks were identified and all of the...
A cracked engine mount of an aircraft was sent to the laboratory to analyze the cause of failure. Dy...
A few fractured bolts recovered from an in flight incident of an aircraft were received for analysi...
Two fractured main landing attachment bolts from an aircraft were sent to the laboratory for analysi...
Two fractured main landing attachment bolts from an aircraft were sent to the laboratory for analysi...
There was an incidence to an aircraft wherein the pilot heard a loud bang on accelerating throttle t...
There was an incidence to an aircraft wherein the pilot heard a loud bang on accelerating throttle t...
Two fractured bolts belonging to an aircraft engine removal ground equipment were brought to the lab...
Two fractured bolts belonging to an aircraft engine removal ground equipment were brought to the lab...
A failed jack attachment bolt belonging to an aircraft was sent to the laboratory for investigation....
Two fractured bolts belonging to an aircraft engine removal ground equipment were brought to the lab...
A failed jack attachment bolt belonging to an aircraft was sent to the laboratory for investigation....
Four failed bolts used in an aircraft were sent to the laboratory for analysis. Examination revealed...
Four failed bolts used in an aircraft were sent to the laboratory for analysis. Examination revealed...
A cracked engine mount of an aircraft was sent to the laboratory to analyze the cause of failure. Dy...
The wheel hub in question has failed by fatigue. Three fatigue cracks were identified and all of the...
A cracked engine mount of an aircraft was sent to the laboratory to analyze the cause of failure. Dy...
A few fractured bolts recovered from an in flight incident of an aircraft were received for analysi...
Two fractured main landing attachment bolts from an aircraft were sent to the laboratory for analysi...
Two fractured main landing attachment bolts from an aircraft were sent to the laboratory for analysi...
There was an incidence to an aircraft wherein the pilot heard a loud bang on accelerating throttle t...
There was an incidence to an aircraft wherein the pilot heard a loud bang on accelerating throttle t...
Two fractured bolts belonging to an aircraft engine removal ground equipment were brought to the lab...
Two fractured bolts belonging to an aircraft engine removal ground equipment were brought to the lab...
A failed jack attachment bolt belonging to an aircraft was sent to the laboratory for investigation....
Two fractured bolts belonging to an aircraft engine removal ground equipment were brought to the lab...
A failed jack attachment bolt belonging to an aircraft was sent to the laboratory for investigation....
Four failed bolts used in an aircraft were sent to the laboratory for analysis. Examination revealed...
Four failed bolts used in an aircraft were sent to the laboratory for analysis. Examination revealed...
A cracked engine mount of an aircraft was sent to the laboratory to analyze the cause of failure. Dy...
The wheel hub in question has failed by fatigue. Three fatigue cracks were identified and all of the...
A cracked engine mount of an aircraft was sent to the laboratory to analyze the cause of failure. Dy...