The impact of the wheelspace cavity purge flow on a high-pressure axial low-reaction turbine stage is investigated. Both the flow's sealing ability and the performance impact associated with its injection are studied. Two operating speeds are tested, namely a high loading case and the peak efficiency, with purge flow rates covering a wide range. As the purge flow is injected upstream of the rotor, the sealing effectiveness is quantified both radially and tangentially close to the rim seal, where the tangential variation is used to identify the seal mixing region. Having passed the rotor blading, the purge flow distribution in the main annulus is quantified, showing an influence of operating speed. The purge flow core is localized to the tra...
An investigation of hot gas ingestion driven by the disc pumping effect in a chute seal was conducte...
This experimental study considered the performance of a chute rim seal downstream of turbine inlet g...
This experimental study considered the performance of a chute rim seal downstream of turbine inlet g...
The impact of the wheelspace cavity purge flow on a high-pressure axial low-reaction turbine stage i...
The area between the stationary and rotating hub side endwall segments in axial turbines is featured...
This paper investigates flow instabilities inside the cavity formed between the stator and rotor dis...
Rim seals throttle flow and have shown to impact the aerodynamic performance of gas turbines. The re...
AbstractIn modern gas turbines, rim seal located between the stator-disc and rotor-disc is used to p...
In modern gas turbines or jet engines, the ingestion of hot gas through the hub-side gap between rot...
This paper is focused on the influence of stator-rotor purge flow injection angle on the aerodynamic...
The present paper investigates the effects of purge flow from a stator-rotor seal gap on the aerodyn...
This paper introduces numerical investigation of a lowspeed linear cascade rig with upstream cavity...
An investigation of hot gas ingestion driven by the disc pumping effect in a chute seal was conducte...
In turbine disk cavity, rim seals are fitted between the stator and its adjacent rotor disk. A coola...
In gas turbine and aeroengine, the rim seal is set between the turbine stator and rotor to prevent i...
An investigation of hot gas ingestion driven by the disc pumping effect in a chute seal was conducte...
This experimental study considered the performance of a chute rim seal downstream of turbine inlet g...
This experimental study considered the performance of a chute rim seal downstream of turbine inlet g...
The impact of the wheelspace cavity purge flow on a high-pressure axial low-reaction turbine stage i...
The area between the stationary and rotating hub side endwall segments in axial turbines is featured...
This paper investigates flow instabilities inside the cavity formed between the stator and rotor dis...
Rim seals throttle flow and have shown to impact the aerodynamic performance of gas turbines. The re...
AbstractIn modern gas turbines, rim seal located between the stator-disc and rotor-disc is used to p...
In modern gas turbines or jet engines, the ingestion of hot gas through the hub-side gap between rot...
This paper is focused on the influence of stator-rotor purge flow injection angle on the aerodynamic...
The present paper investigates the effects of purge flow from a stator-rotor seal gap on the aerodyn...
This paper introduces numerical investigation of a lowspeed linear cascade rig with upstream cavity...
An investigation of hot gas ingestion driven by the disc pumping effect in a chute seal was conducte...
In turbine disk cavity, rim seals are fitted between the stator and its adjacent rotor disk. A coola...
In gas turbine and aeroengine, the rim seal is set between the turbine stator and rotor to prevent i...
An investigation of hot gas ingestion driven by the disc pumping effect in a chute seal was conducte...
This experimental study considered the performance of a chute rim seal downstream of turbine inlet g...
This experimental study considered the performance of a chute rim seal downstream of turbine inlet g...