An investigation has teen made in the Langley high-speed 7- by 10-”foot tunnel using the trensonic-bumy method to determine the longitudinal stability end control characteristics at transonic speeds of a semispan airplane model having a 45 ° sveptback wing and tail. The results of the investigation indicated an increase in the rate of change of pitching-moment coefficient with lift coefficient at a L)a-cmconstant Mach number-E ~ through the transonic range that was attributed to a rearward snift of the wing-fuselage aerodynamic-center location at subsonic speeds and to a rapid decrease in dowmwash at supersonic speeds. At a Mach number of about 0.95 a moderate decrease occurred in both the lift-curve slope and in the stabilizer effectivenes...
A preliminary investigation of the static longitudinal and lateral stability characteristics of a 0....
An investigation was made by the NACA wing-flow method to determine the drag, pitching-moment, lift,...
An investigation was made in the Langley high-speed 7- hy 10-foot tunnel to determine the feasibilit...
An investigation of the longitudinal stability and of the all-movable horizontal tail and aileron co...
This report presents the results of an investigation in the transonic speed range of the longitudina...
The transonic longitudinal aerodynamic characteristics of a 0.0858-scale model of the Lockheed XF-10...
A comprehensive investigation of the aerodynamic characteristics of various configurations of a 1/22...
Transonic wind tunnel study of static longitudinal and lateral stability and control characteristics...
An investigation was made in the high Mach number test section of the Langley Unitary Plan wind tunn...
The longitudinal stability and control characteristics of a 1/30-scale model of the Republic XF-103 ...
An investigation by the transonic-bump technique of the static longitudinal aerodynamic characterist...
The results of transonic flight measurements of the longitudinal stability characteristics of the Do...
The longitudinal stability and control characteristics of a 1/30-scale model of the Republic XF-103 ...
The longitudinal aerodynamic characteristics of a wing-body-horizontal-tail configuration designed f...
The effects of elevator deflections from 0deg to -20deg on the force and moment characteristics of a...
A preliminary investigation of the static longitudinal and lateral stability characteristics of a 0....
An investigation was made by the NACA wing-flow method to determine the drag, pitching-moment, lift,...
An investigation was made in the Langley high-speed 7- hy 10-foot tunnel to determine the feasibilit...
An investigation of the longitudinal stability and of the all-movable horizontal tail and aileron co...
This report presents the results of an investigation in the transonic speed range of the longitudina...
The transonic longitudinal aerodynamic characteristics of a 0.0858-scale model of the Lockheed XF-10...
A comprehensive investigation of the aerodynamic characteristics of various configurations of a 1/22...
Transonic wind tunnel study of static longitudinal and lateral stability and control characteristics...
An investigation was made in the high Mach number test section of the Langley Unitary Plan wind tunn...
The longitudinal stability and control characteristics of a 1/30-scale model of the Republic XF-103 ...
An investigation by the transonic-bump technique of the static longitudinal aerodynamic characterist...
The results of transonic flight measurements of the longitudinal stability characteristics of the Do...
The longitudinal stability and control characteristics of a 1/30-scale model of the Republic XF-103 ...
The longitudinal aerodynamic characteristics of a wing-body-horizontal-tail configuration designed f...
The effects of elevator deflections from 0deg to -20deg on the force and moment characteristics of a...
A preliminary investigation of the static longitudinal and lateral stability characteristics of a 0....
An investigation was made by the NACA wing-flow method to determine the drag, pitching-moment, lift,...
An investigation was made in the Langley high-speed 7- hy 10-foot tunnel to determine the feasibilit...