A wind-tunnel investigation was made at low speed to detemine the aerodynamic characteristics of a hs ” sweptback untapered semispan wing of NACA 64.Ao1oairfoil section normal to the leading edge and aspect ratio of 1.59 equipped with 2~-percent-chordplain unsealed flaps having various spans and spanwise locations. Ltit, drag, pitching-moment, and flap hinge-moment data were obtained for the wing with the various flaps-deflectedup to 600. A comparison is ~de with data obtained on the present wing at 0 ° of sweep with an aspect ratio of 3.13. In general, changes in angle of attack, flap deflection, flap span, and spanwise location produced trends in lift, drag; pitching moment, and flap hinge moment that were similar to but of different magn...
A small-scale transonic investigation of two semispan wings of the same plan form was made in the La...
Aerodynamic force tests were made in the N.A.C.A. 7 by 10 foot wind tunnel on a model Clark Y wing w...
A low-speed wind-tunnel investigation was made to determine the lateral control characteristics of a...
Force and moment data were obtained at low speeds to determine the aerodynamic characteristics of an...
An investigation was conducted in the NACA 19-foot pressure wind tunnel of a rectangular wing having...
An investigation has been made at large scale of the characteristics of highly swept wings. Data wer...
The incremental l i f t and pitching moments produced by 20-percent-chord s p l i t f l a p s of va...
The effects of deflecting full-span, constant-chord, leading-edge flaps, having either round or shar...
Tests were made on a model wing with three different sized split trailing-edged flaps, in the NACA 7...
S~*(ARY Lift, drag and pitching moment have been measured over an extensive range of configurations ...
The investigation was made to determine the effects of full-span and of partial-span split flaps on ...
An investigation was made to determine the aerodynamic characteristics of tapered and rectangular wi...
An investigation was conducted in the NACA 19-foot pressure wind tunnel of a tapered wing with strai...
Results of wind-tunnel tests of a semispan model of a triangular wing of aspect ratio 2 with a skewe...
An investigation has been made in the NACA 7- by 10-foot wind tunnel of a large chord NACA 23021 air...
A small-scale transonic investigation of two semispan wings of the same plan form was made in the La...
Aerodynamic force tests were made in the N.A.C.A. 7 by 10 foot wind tunnel on a model Clark Y wing w...
A low-speed wind-tunnel investigation was made to determine the lateral control characteristics of a...
Force and moment data were obtained at low speeds to determine the aerodynamic characteristics of an...
An investigation was conducted in the NACA 19-foot pressure wind tunnel of a rectangular wing having...
An investigation has been made at large scale of the characteristics of highly swept wings. Data wer...
The incremental l i f t and pitching moments produced by 20-percent-chord s p l i t f l a p s of va...
The effects of deflecting full-span, constant-chord, leading-edge flaps, having either round or shar...
Tests were made on a model wing with three different sized split trailing-edged flaps, in the NACA 7...
S~*(ARY Lift, drag and pitching moment have been measured over an extensive range of configurations ...
The investigation was made to determine the effects of full-span and of partial-span split flaps on ...
An investigation was made to determine the aerodynamic characteristics of tapered and rectangular wi...
An investigation was conducted in the NACA 19-foot pressure wind tunnel of a tapered wing with strai...
Results of wind-tunnel tests of a semispan model of a triangular wing of aspect ratio 2 with a skewe...
An investigation has been made in the NACA 7- by 10-foot wind tunnel of a large chord NACA 23021 air...
A small-scale transonic investigation of two semispan wings of the same plan form was made in the La...
Aerodynamic force tests were made in the N.A.C.A. 7 by 10 foot wind tunnel on a model Clark Y wing w...
A low-speed wind-tunnel investigation was made to determine the lateral control characteristics of a...