A flight test of the Aero jet Engineering Corporation's 75-6000 T-27 Jato rocket motor was conducted at the Langley Pilotless Aircraft Research Station at Wallops Island, Va, to determine the flight-performance characteristics of the motor. The flight test imposed an absolute longitudinal acceleration of 9.8g upon the rocket motor at 2.8 seconds after launching. The total impulse developed by the motor was 43,400 pound-seconds, and the thrusting time was 7.58 secoads. The maximum thrust was 7200 pounds and occurred at 4.8 seconds after launching. No thrust irregularities attributable to effects of the flight longitudinal acceleration were observed. Certain small t m s t irregularities occurred in the flight test which appear to corresp...
A flight investigation was made of a rocket-launched ram-jet engine incorporating an inlet designed ...
Experience accumulated during the past 10 years in measuring turbojet-engine thrust in altitude faci...
A general description of the design and construction of the WASP sounding rocket and of the performa...
Flight tests were conducted at the NACA Pilotless Aircraft Research Station, Wallops Island, to dete...
Flight tests were conducted at the NACA Pilotless Aircraft Research Station, Wallops Island, to dete...
Since there is a dearth of flight vibration data and because of the current wide interest in solid-p...
Nowadays a lot of research is done in the field of electromagnetic driven Lorentz Rail Accelerators ...
A successful flight test of a spin-stabilized 20-inch-diameter solid-propellant rocket motor having ...
A force balance system for measuring lift, thrust and pitching moment has been used to measure the p...
An experiment was performed to measure the impulse of the A8-3 Estes model rocket engine. The measur...
Scientific and Technical Information Office 1980 SUMMARY A hydrogen-peroxide-fueled rocket system wa...
Low-speed tests of a pilotless aircraft were conducted in the Langley propeller-research tunnel to p...
A free-flight investigation over a Mach number range from 0.6 to 2.0 has been conducted to determine...
Hypresearch is a project that has been under development with the collaboration of ATG Europe, TU De...
Integrated rocket ramjet engine is adapted to aircraft propulsion and supersonic missiles moving at ...
A flight investigation was made of a rocket-launched ram-jet engine incorporating an inlet designed ...
Experience accumulated during the past 10 years in measuring turbojet-engine thrust in altitude faci...
A general description of the design and construction of the WASP sounding rocket and of the performa...
Flight tests were conducted at the NACA Pilotless Aircraft Research Station, Wallops Island, to dete...
Flight tests were conducted at the NACA Pilotless Aircraft Research Station, Wallops Island, to dete...
Since there is a dearth of flight vibration data and because of the current wide interest in solid-p...
Nowadays a lot of research is done in the field of electromagnetic driven Lorentz Rail Accelerators ...
A successful flight test of a spin-stabilized 20-inch-diameter solid-propellant rocket motor having ...
A force balance system for measuring lift, thrust and pitching moment has been used to measure the p...
An experiment was performed to measure the impulse of the A8-3 Estes model rocket engine. The measur...
Scientific and Technical Information Office 1980 SUMMARY A hydrogen-peroxide-fueled rocket system wa...
Low-speed tests of a pilotless aircraft were conducted in the Langley propeller-research tunnel to p...
A free-flight investigation over a Mach number range from 0.6 to 2.0 has been conducted to determine...
Hypresearch is a project that has been under development with the collaboration of ATG Europe, TU De...
Integrated rocket ramjet engine is adapted to aircraft propulsion and supersonic missiles moving at ...
A flight investigation was made of a rocket-launched ram-jet engine incorporating an inlet designed ...
Experience accumulated during the past 10 years in measuring turbojet-engine thrust in altitude faci...
A general description of the design and construction of the WASP sounding rocket and of the performa...