The Director of the NASA Engineering and Safety Center (NESC), requested an independent assessment of the anomalous gaseous hydrogen (GH2) flow incident on the Space Shuttle Program (SSP) Orbiter Vehicle (OV)-105 during the Space Transportation System (STS)-126 mission. The main propulsion system (MPS) engine #2 GH2 flow control valve (FCV) LV-57 transition from low towards high flow position without being commanded. Post-flight examination revealed that the FCV LV-57 poppet had experienced a fatigue failure that liberated a section of the poppet flange. The NESC assessment provided a peer review of the computational fluid dynamics (CFD), stress analysis, and impact testing. A probability of detection (POD) study was requested by the SSP Or...
A number of the accidents/incidents with hydrogen in NASA operations are reviewed. The cause factors...
A recent identification of cracking in the Space Shuttle Primary Reaction Control System (PRCS) thru...
A significant anomaly, Fuel Valve Pilot Seal Extrusion, is affecting the Shuttle Primary Reaction Co...
The Director of the NASA Engineering and Safety Center (NESC), requested an independent assessment o...
The presentation examines the background and objective of nondestructive crack detection, flow contr...
The Alternative Fuel Effects on Contrails and Cruise Emissions (ACCESS) Project Integration Manager ...
Space Shuttle Main Engines (SSME) discharge a significant quantity of unburned hydrogen during norma...
Since the loss of Columbia on February 1, 2003, the Space Shuttle Program (SSP) has significantly im...
The Alternative Fuel Effects on Contrails & Cruise Emissions (ACCESS) Project Integration Manager re...
Work performed by Southwest Research Institute (SwRI) as part of an Independent Technical Assessment...
As part of the health assessment of flight spare 40in diameter Kevlar composite overwrapped pressure...
An abbreviated program was conducted to investigate igniter, injector, and thrust chamber technology...
Technology for long life, high performing, gaseous hydrogen-gaseous oxygen rocket engines suitable f...
High-energy cryogenic propellant is an essential element in future space exploration programs. There...
The Transient Cryogen Transfer Computer Program (TCTP) developed and verified for LOX systems by ana...
A number of the accidents/incidents with hydrogen in NASA operations are reviewed. The cause factors...
A recent identification of cracking in the Space Shuttle Primary Reaction Control System (PRCS) thru...
A significant anomaly, Fuel Valve Pilot Seal Extrusion, is affecting the Shuttle Primary Reaction Co...
The Director of the NASA Engineering and Safety Center (NESC), requested an independent assessment o...
The presentation examines the background and objective of nondestructive crack detection, flow contr...
The Alternative Fuel Effects on Contrails and Cruise Emissions (ACCESS) Project Integration Manager ...
Space Shuttle Main Engines (SSME) discharge a significant quantity of unburned hydrogen during norma...
Since the loss of Columbia on February 1, 2003, the Space Shuttle Program (SSP) has significantly im...
The Alternative Fuel Effects on Contrails & Cruise Emissions (ACCESS) Project Integration Manager re...
Work performed by Southwest Research Institute (SwRI) as part of an Independent Technical Assessment...
As part of the health assessment of flight spare 40in diameter Kevlar composite overwrapped pressure...
An abbreviated program was conducted to investigate igniter, injector, and thrust chamber technology...
Technology for long life, high performing, gaseous hydrogen-gaseous oxygen rocket engines suitable f...
High-energy cryogenic propellant is an essential element in future space exploration programs. There...
The Transient Cryogen Transfer Computer Program (TCTP) developed and verified for LOX systems by ana...
A number of the accidents/incidents with hydrogen in NASA operations are reviewed. The cause factors...
A recent identification of cracking in the Space Shuttle Primary Reaction Control System (PRCS) thru...
A significant anomaly, Fuel Valve Pilot Seal Extrusion, is affecting the Shuttle Primary Reaction Co...