A transonic axial-flow-compressor rotor was tested w i t h low blade angles. The rotor contained the blades used i n a previous investi&tion, but they were set i n a new rotor disk a t a setting angle 8 closer to the axial direct ion than in the original rotor. Over-all and blade-element performance of the low-blade-angle rotor are given herein. The perform-rotor data. I ance is compared with the original rotor and other t ansonic-compressor A t a corrected speed of 1loo feet per second, the low-blade-angle rotor operated w i t h a re la t ive inlet m c h number of 1.2, a diffusion factor of 0.65, and an axial veloci ty ra t io of 0.71 i n the t i p region (11 percent of the passage height away from the outer W ~ J L L). The meas-ured ...
An analytical and experimental study of the performance changes and flow effects of rotor tip cleara...
An analytical and experimental study of the performance changes and flow effects of rotor tip cleara...
A three-dimensional computation was conducted to understand effects of low Reynolds numbers on loss ...
At a corrected speed of 1100 feet per second, the low-blade-angle rotor operated with a relative inl...
Performance data are presented for a transonic axial-flow compressor rotor designed to operate at a ...
This study investigates the aerodynamic and aeroelastic characteristics of a transonic axial compres...
In order to determine the effect of a low design diffusion factor on the performance of a transonic ...
Performance data are presented for a transonic axial-flow compressor rotor designed to operate at a ...
A typical axial-flow compressor rotor using NACA 65-series compressor blades was tested at low speed...
The experimental performance of a 20-inch-diameter axial-flow transonic compressor rotor with small ...
A systematic investigation to understand the impact of axial sweep and tangential lean on the aerody...
A systematic investigation to understand the impact of axial sweep and tangential lean on the aerody...
In this paper, the impact of manufacturing variations on performance of an axial compressor rotor ar...
In this paper, the impact of manufacturing variations on performance of an axial compressor rotor is...
An analytical and experimental study of the performance changes and flow effects of rotor tip cleara...
An analytical and experimental study of the performance changes and flow effects of rotor tip cleara...
An analytical and experimental study of the performance changes and flow effects of rotor tip cleara...
A three-dimensional computation was conducted to understand effects of low Reynolds numbers on loss ...
At a corrected speed of 1100 feet per second, the low-blade-angle rotor operated with a relative inl...
Performance data are presented for a transonic axial-flow compressor rotor designed to operate at a ...
This study investigates the aerodynamic and aeroelastic characteristics of a transonic axial compres...
In order to determine the effect of a low design diffusion factor on the performance of a transonic ...
Performance data are presented for a transonic axial-flow compressor rotor designed to operate at a ...
A typical axial-flow compressor rotor using NACA 65-series compressor blades was tested at low speed...
The experimental performance of a 20-inch-diameter axial-flow transonic compressor rotor with small ...
A systematic investigation to understand the impact of axial sweep and tangential lean on the aerody...
A systematic investigation to understand the impact of axial sweep and tangential lean on the aerody...
In this paper, the impact of manufacturing variations on performance of an axial compressor rotor ar...
In this paper, the impact of manufacturing variations on performance of an axial compressor rotor is...
An analytical and experimental study of the performance changes and flow effects of rotor tip cleara...
An analytical and experimental study of the performance changes and flow effects of rotor tip cleara...
An analytical and experimental study of the performance changes and flow effects of rotor tip cleara...
A three-dimensional computation was conducted to understand effects of low Reynolds numbers on loss ...