A spin investigation has been conducted in the Langley 20-foot free-spinning tunnel on a 1/24-scale model of the North American XP-86 airplane. The effects of control settings and movements upon the erect and inverted spin and recovery characteristics of the model were determined for the design gross weight loading. The long-range loading was also investigated and the effects of extending slats and dive flaps were determined. In addition, the investigation included the determination of the size of spin-recovery parachute required for emergency recovery from demonstration spins, the rudder force required to move the rudder for recovery, and the best method for the pilot to escape if it should become necessary to do so during a spin. The resu...
A spin-recovery investigation has been conducted in the Langley 20-foot free-spinning tunnel on a 20...
A spin-tunnel investigation of a 1/26 scale model of the Douglas XTB2D-1 airplane has been conducted...
An investigation has been conducted in the Langley 20-foot free-spinning tunnel to determine the eff...
A spin investigation has been conducted in the Langley 20-foot free-spinning tunnel on a 1/24-scale ...
An investigation of the spin and recovery characteristics of a scale model of the Grumman XF9F-2 air...
An investigation of the spin and recovery characteristics of a 0.057-scale model of the Chance Vough...
An investigation of the spin and recovery characteristics of a 1/24-scale model of the Grumman AF-2S...
A supplementary investigation has been conducted in the Langley 20-foot free-spinning tunnel of a l/...
In accordance with a request of the Bureau of Aeronautics, Navy Department, tests were performed in ...
Spin tests have been performed in the Langley 20-foot free-spinning tunnel on a 1/18-scale model of ...
A spin investigation has been conducted in the Langley 20-foot free-spinning tunnel on a 1/20-scale ...
An investigation has been conducted i n the Langley 20-foot free-spinning tunnel on a 1/25-scale mod...
A spin-recovery investigation has been conducted in the Langley 20-foot free-spinning tunnel on a 20...
A spin-tunnel investigation of a 1/26 scale model of the Douglas XTB2D-1 airplane has been conducted...
An investigation has been conducted in the Langley 20-foot free-spinning tunnel to determine the eff...
A spin investigation has been conducted in the Langley 20-foot free-spinning tunnel on a 1/24-scale ...
An investigation of the spin and recovery characteristics of a scale model of the Grumman XF9F-2 air...
An investigation of the spin and recovery characteristics of a 0.057-scale model of the Chance Vough...
An investigation of the spin and recovery characteristics of a 1/24-scale model of the Grumman AF-2S...
A supplementary investigation has been conducted in the Langley 20-foot free-spinning tunnel of a l/...
In accordance with a request of the Bureau of Aeronautics, Navy Department, tests were performed in ...
Spin tests have been performed in the Langley 20-foot free-spinning tunnel on a 1/18-scale model of ...
A spin investigation has been conducted in the Langley 20-foot free-spinning tunnel on a 1/20-scale ...
An investigation has been conducted i n the Langley 20-foot free-spinning tunnel on a 1/25-scale mod...
A spin-recovery investigation has been conducted in the Langley 20-foot free-spinning tunnel on a 20...
A spin-tunnel investigation of a 1/26 scale model of the Douglas XTB2D-1 airplane has been conducted...
An investigation has been conducted in the Langley 20-foot free-spinning tunnel to determine the eff...